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IAC Assessment: ME0268
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IAC Assessment: ME0268
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IAC Center University of Maine
Assessment Year 1999
Principal Product Poker Chips
NAICS n/a
SIC 3944 - Games, Toys, and Children's Vehicles, Except Dolls and Bicycles
Sales $1,000,000-$5,000,000
# of Employees 33
Plant Area (Sq.Ft.) 83,000
Annual Production 4,000,000 Pieces
Production Hrs. Annual 2,250
Location (State) ME
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $15,220 204,279 kWh $0.07
Electricity Demand $6,518 750 kW-months/year $8.69
Electricity Fees $1,348 - $ -
LPG $8,730 945 MMBtu $9.24
TOTAL ENERGY COSTS $31,816
RECOMMENDED SAVINGS* $6,537 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $5,533
#|Description Savings
Cost
Status Electricity Usage Electricity Demand LPG Administrative Changes Electricity Usage Electricity Demand LPG Administrative Changes
$ kWh $ kW-months/year $ MMBtu $ $
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$1,554
Cost:
$4,763
$994 13,189 $560 70 - - - - $994
13,189
kWh
$560
70
kW-months/year
-
-
MMBtu
-
-
$
02: 4.811 DEMOLISH OLD BUILDING TO REDUCE TAX AND INSURANCE BILLS Savings:
$1,000
Cost:
-
- - - - - - $1,000 - -
-
kWh
-
-
kW-months/year
-
-
MMBtu
$1,000
-
$
03: 4.211 CONSIDER USE / PURCHASE OF BULK MATERIALS WHERE POSSIBLE Savings:
$860
Cost:
-
- - - - - - $860 - -
-
kWh
-
-
kW-months/year
-
-
MMBtu
$860
-
$
04: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT Savings:
$697
Cost:
$300
$672 9,672 $435 5 $(-410) (-44) - - $672
9,672
kWh
$435
5
kW-months/year
$(-410)
(-44)
MMBtu
-
-
$
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$568
Cost:
$250
$568 8,206 - - - - - - $568
8,206
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
$
06: 2.2511 INSULATE BARE EQUIPMENT Savings:
$567
Cost:
$54
$567 4,982 - - - - - - $567
4,982
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
$
07: 4.652 REPLACE EXISTING EQUIPMENT WITH MORE SUITABLE SUBSTITUTES Savings:
$355
Cost:
$980
$355 4,689 - - - - - - $355
4,689
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
$
08: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$338
Cost:
$482
$338 4,103 - - - - - - $338
4,103
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
$
09: 4.821 PAY BILLS ON TIME TO AVOID LATE FEES Savings:
$281
Cost:
-
- - - - - - $281 - -
-
kWh
-
-
kW-months/year
-
-
MMBtu
$281
-
$
10: 2.8121 APPLY FOR TAX-FREE STATUS FOR ENERGY PURCHASES Savings:
$186
Cost:
-
- - - - - - $186 - -
-
kWh
-
-
kW-months/year
-
-
MMBtu
$186
-
$
11: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS Savings:
$82
Cost:
$100
$82 1,172 - - - - - - $82
1,172
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
$
12: 4.821 PAY BILLS ON TIME TO AVOID LATE FEES Savings:
$49
Cost:
-
- - - - - - $49 - -
-
kWh
-
-
kW-months/year
-
-
MMBtu
$49
-
$
TOTAL RECOMMENDED Savings:
$6,537
Cost:
$6,929
$3,576 46,013 $995 75 $(-410) (-44) $2,376 - $3,576
46,013
kWh
$995
75
kW-months/year
$(-410)
(-44)
MMBtu
$2,376
-
$
TOTAL IMPLEMENTED Savings:
$5,533
Cost:
$5,795
$2,572 35,170 $995 75 $(-410) (-44) $2,376 - $2,572
35,170
kWh
$995
75
kW-months/year
$(-410)
(-44)
MMBtu
$2,376
-
$
Savings
Cost
$ kWh $ kW-months/year $ MMBtu $ $
Electricity Usage Electricity Demand LPG Administrative Changes Electricity Usage Electricity Demand LPG Administrative Changes