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IAC Assessment: OK0178
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IAC Assessment: OK0178
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Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
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IAC Center Oklahoma State University
Assessment Year 1985
Principal Product PLATED & ANODIZED METAL
NAICS n/a
SIC 3471 - Plating And Polishing
Sales $1,000,000-$5,000,000
# of Employees 62
Plant Area (Sq.Ft.) 0
Annual Production 0 Units
Production Hrs. Annual 4,420
Location (State) OK
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $51,631 917,644 kWh $0.06
Natural Gas $54,834 14,410 MMBtu $3.81
TOTAL ENERGY COSTS $106,465
RECOMMENDED SAVINGS* $14,107 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $3,989
#|Description Savings
Cost
Status Electricity Usage Natural Gas LPG Administrative Changes Electricity Usage Natural Gas LPG Administrative Changes
$ kWh $ MMBtu $ MMBtu $ $
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$2,258
Cost:
$800
- - $2,318 609 - - $(-60) - -
-
kWh
$2,318
609
MMBtu
-
-
MMBtu
$(-60)
-
$
02: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$1,524
Cost:
$4,000
- - $1,524 400 - - - - -
-
kWh
$1,524
400
MMBtu
-
-
MMBtu
-
-
$
03: 2.7231 USE RADIANT HEATER FOR SPOT HEATING Savings:
$1,400
Cost:
$2,120
- - $2,099 551 $(-699) (-92) - - -
-
kWh
$2,099
551
MMBtu
$(-699)
(-92)
MMBtu
-
-
$
04: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS Savings:
$178
Cost:
$150
- - $178 47 - - - - -
-
kWh
$178
47
MMBtu
-
-
MMBtu
-
-
$
05: 2.2514 COVER OPEN TANKS Savings:
$5,600
Cost:
$9,888
- - $5,600 1,470 - - - - -
-
kWh
$5,600
1,470
MMBtu
-
-
MMBtu
-
-
$
06: 2.2511 INSULATE BARE EQUIPMENT Savings:
$1,732
Cost:
$636
- - $1,732 455 - - - - -
-
kWh
$1,732
455
MMBtu
-
-
MMBtu
-
-
$
07: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME Savings:
$244
Cost:
$200
$244 3,810 - - - - - - $244
3,810
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
08: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS Savings:
$64
Cost:
$55
$64 1,758 - - - - - - $64
1,758
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
09: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$528
Cost:
$1,795
$528 - - - - - - - $528
-
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
10: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$579
Cost:
$250
$579 9,965 - - - - - - $579
9,965
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$14,107
Cost:
$19,894
$1,415 15,533 $13,451 3,532 $(-699) (-92) $(-60) - $1,415
15,533
kWh
$13,451
3,532
MMBtu
$(-699)
(-92)
MMBtu
$(-60)
-
$
TOTAL IMPLEMENTED Savings:
$3,989
Cost:
$6,775
$887 15,533 $3,801 998 $(-699) (-92) - - $887
15,533
kWh
$3,801
998
MMBtu
$(-699)
(-92)
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ MMBtu $ $
Electricity Usage Natural Gas LPG Administrative Changes Electricity Usage Natural Gas LPG Administrative Changes