Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oklahoma State University |
---|---|
Assessment Year | 1991 |
Principal Product | AIRCRAFT PARTS |
NAICS | n/a |
SIC | 3728 - Aircraft Parts And Equipment, Nec |
Sales | $50,000,000-$100,000,000 |
# of Employees | 850 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 1,265,000 Pieces |
Production Hrs. Annual | 4,000 |
Location (State) | OK |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $703,199 | 14,726,260 | kWh | $0.05 |
Natural Gas | $202,259 | 89,068 | MMBtu | $2.27 |
TOTAL ENERGY COSTS | $905,458 | |||
RECOMMENDED SAVINGS* | $39,775 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS |
Savings: $3,574 Cost: $1,300 |
- | - | $3,574 | 1,733 | - | - |
- - kWh |
$3,574 1,733 MMBtu |
- - $ |
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02: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $9,981 Cost: $2,550 |
- | - | $9,981 | 4,845 | - | - |
- - kWh |
$9,981 4,845 MMBtu |
- - $ |
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03: 2.6232 INSTALL SET-BACK TIMERS |
Savings: $162 Cost: $330 |
$162 | 4,689 | - | - | - | - |
$162 4,689 kWh |
- - MMBtu |
- - $ |
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04: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $8,525 Cost: $25,022 |
$8,525 | 241,794 | - | - | - | - |
$8,525 241,794 kWh |
- - MMBtu |
- - $ |
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05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $16,499 Cost: $35,947 |
$16,499 | 313,599 | - | - | - | - |
$16,499 313,599 kWh |
- - MMBtu |
- - $ |
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06: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $914 Cost: - |
$1,064 | 30,188 | - | - | $(-150) | - |
$1,064 30,188 kWh |
- - MMBtu |
$(-150) - $ |
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07: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $120 Cost: - |
$305 | 6,448 | - | - | $(-185) | - |
$305 6,448 kWh |
- - MMBtu |
$(-185) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $39,775 Cost: $65,149 |
$26,555 | 596,718 | $13,555 | 6,578 | $(-335) | - | $26,555 596,718 kWh |
$13,555 6,578 MMBtu |
$(-335) - $ |
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TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - | - | - - kWh |
- - MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |