Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oklahoma State University |
---|---|
Assessment Year | 1992 |
Principal Product | TRAILERS, HORSE & CATTLE |
NAICS | n/a |
SIC | 3799 - Transportation Equipment, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 200 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 1,820 Pieces |
Production Hrs. Annual | 2,080 |
Location (State) | OK |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $81,753 | 1,138,042 | kWh | $0.07 |
LPG | $8,131 | 1,007 | MMBtu | $8.07 |
TOTAL ENERGY COSTS | $89,884 | |||
RECOMMENDED SAVINGS* | $6,879 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $5,709 |
#|Description |
Savings Cost |
Status | Electricity Usage | LPG | Administrative Changes | Electricity Usage | LPG | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $3,222 Cost: $3,222 |
$3,372 | 64,478 | - | - | $(-150) | - |
$3,372 64,478 kWh |
- - MMBtu |
$(-150) - $ |
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02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $782 Cost: $782 |
$1,017 | 19,343 | - | - | $(-235) | - |
$1,017 19,343 kWh |
- - MMBtu |
$(-235) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS |
Savings: $1,133 Cost: $1,133 |
$1,133 | 21,688 | - | - | - | - |
$1,133 21,688 kWh |
- - MMBtu |
- - $ |
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04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $777 Cost: $777 |
$777 | 14,947 | - | - | - | - |
$777 14,947 kWh |
- - MMBtu |
- - $ |
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05: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS |
Savings: $388 Cost: $388 |
$388 | 7,327 | - | - | - | - |
$388 7,327 kWh |
- - MMBtu |
- - $ |
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06: 2.6214 SHUT OFF PILOTS IN STANDBY EQUIPMENT |
Savings: $388 Cost: $561 |
- | - | $388 | 48 | - | - |
- - kWh |
$388 48 MMBtu |
- - $ |
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07: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $189 Cost: $554 |
$189 | 3,517 | - | - | - | - |
$189 3,517 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $6,879 Cost: $7,417 |
$6,876 | 131,300 | $388 | 48 | $(-385) | - | $6,876 131,300 kWh |
$388 48 MMBtu |
$(-385) - $ |
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TOTAL IMPLEMENTED |
Savings: $5,709 Cost: $6,074 |
$5,859 | 111,957 | - | - | $(-150) | - | $5,859 111,957 kWh |
- - MMBtu |
$(-150) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | LPG | Administrative Changes | Electricity Usage | LPG | Administrative Changes |