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IAC Assessment: OK0387
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IAC Assessment: OK0387
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IAC Center Oklahoma State University
Assessment Year 1992
Principal Product STAINLESS STEEL TUBING
NAICS n/a
SIC 3317 - Steel Pipe And Tubes
Sales $10,000,000-$50,000,000
# of Employees 56
Plant Area (Sq.Ft.) 0
Annual Production 21,000 Thousand Feet
Production Hrs. Annual 8,736
Location (State) OK
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $187,896 2,980,363 kWh $0.06
Natural Gas $7,129 1,327 MMBtu $5.37
TOTAL ENERGY COSTS $195,025
RECOMMENDED SAVINGS* $31,156 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $24,791
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.4239 ELIMINATE OR REDUCE COMPRESSED AIR USAGE Savings:
$20,408
Cost:
$1,580
$20,408 375,733 - - - - $20,408
375,733
kWh
-
-
MMBtu
-
-
$
02: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$5,003
Cost:
$8,297
$5,003 101,407 - - - - $5,003
101,407
kWh
-
-
MMBtu
-
-
$
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$2,457
Cost:
$1,131
$3,283 62,134 - - $(-826) - $3,283
62,134
kWh
-
-
MMBtu
$(-826)
-
$
04: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$1,087
Cost:
$1,276
$1,087 20,516 - - - - $1,087
20,516
kWh
-
-
MMBtu
-
-
$
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$832
Cost:
-
$832 20,809 - - - - $832
20,809
kWh
-
-
MMBtu
-
-
$
06: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$615
Cost:
$2,279
$615 12,309 - - - - $615
12,309
kWh
-
-
MMBtu
-
-
$
07: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$612
Cost:
$1,922
- - $612 115 - - -
-
kWh
$612
115
MMBtu
-
-
$
08: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$135
Cost:
$318
$135 2,052 - - - - $135
2,052
kWh
-
-
MMBtu
-
-
$
09: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$7
Cost:
$111
$21 293 - - $(-14) - $21
293
kWh
-
-
MMBtu
$(-14)
-
$
TOTAL RECOMMENDED Savings:
$31,156
Cost:
$16,914
$31,384 595,253 $612 115 $(-840) - $31,384
595,253
kWh
$612
115
MMBtu
$(-840)
-
$
TOTAL IMPLEMENTED Savings:
$24,791
Cost:
$4,098
$25,631 479,485 - - $(-840) - $25,631
479,485
kWh
-
-
MMBtu
$(-840)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes