Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oklahoma State University |
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Assessment Year | 1996 |
Principal Product | Cooked sausages, hams, and meats |
NAICS | n/a |
SIC | 2013 - Sausages And Other Prepared Meats |
Sales | $5,000,000-$10,000,000 |
# of Employees | 50 |
Plant Area (Sq.Ft.) | 33,000 |
Annual Production | 4,500,000 Pounds |
Production Hrs. Annual | 2,340 |
Location (State) | OK |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $31,220 | 1,065,651 | kWh | $0.03 |
Electricity Demand | $29,690 | 2,808 | kW-months/year | $10.57 |
Electricity Fees | $3,250 | - | $ | - |
Natural Gas | $15,756 | 4,405 | MMBtu | $3.58 |
TOTAL ENERGY COSTS | $89,456 | |||
RECOMMENDED SAVINGS* | $10,927 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $189 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Water Disposal | Electricity Usage | Natural Gas | Water Disposal | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | Tgal | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.1221 REPLACE OBSOLETE BURNERS WITH MORE EFFICIENT ONES |
Savings: $10,738 Cost: $10,000 |
- | - | $10,738 | 2,456 | - | - |
- - kWh |
$10,738 2,456 MMBtu |
- - Tgal |
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02: 2.4314 USE SYNTHETIC LUBRICANT |
Savings: $90 Cost: $155 |
$90 | 3,224 | - | - | - | - |
$90 3,224 kWh |
- - MMBtu |
- - Tgal |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 3.1194 USE AUTOMATIC FLOW CONTROL |
Savings: $16 Cost: $46 |
- | - | - | - | $16 | 3,500 |
- - kWh |
- - MMBtu |
$16 3,500 Tgal |
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04: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $83 Cost: $30 |
$83 | 4,689 | - | - | - | - |
$83 4,689 kWh |
- - MMBtu |
- - Tgal |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $10,927 Cost: $10,231 |
$173 | 7,913 | $10,738 | 2,456 | $16 | 3,500 | $173 7,913 kWh |
$10,738 2,456 MMBtu |
$16 3,500 Tgal |
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TOTAL IMPLEMENTED |
Savings: $189 Cost: $231 |
$173 | 7,913 | - | - | $16 | 3,500 | $173 7,913 kWh |
- - MMBtu |
$16 3,500 Tgal |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | Tgal | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Water Disposal | Electricity Usage | Natural Gas | Water Disposal |