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IAC Assessment: OK0940
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IAC Assessment: OK0940
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
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IAC Center Oklahoma State University
Assessment Year 2016
Principal Product Solid rubber tires/wheel assemblies
NAICS 326211 - Tire Manufacturing (except Retreading)
SIC 3011 - Tires And Inner Tubes
Sales $10,000,000-$50,000,000
# of Employees 100
Plant Area (Sq.Ft.) 300,000
Annual Production 7,000,000 Pounds
Production Hrs. Annual 2,860
Location (State) OK
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $257,603 3,416,842 kWh $0.08
Natural Gas $110,658 30,961 MMBtu $3.57
TOTAL ENERGY COSTS $368,261
RECOMMENDED SAVINGS* $33,768 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $6,364
#|Description Savings
Cost
Status Electricity Usage Electricity Fees Natural Gas Electricity Usage Electricity Fees Natural Gas
$ kWh $ $ $ MMBtu
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$7,811
Cost:
$17,000
- - - - $7,811 2,177 -
-
kWh
-
-
$
$7,811
2,177
MMBtu
02: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$1,586
Cost:
$7,700
- - - - $1,586 442 -
-
kWh
-
-
$
$1,586
442
MMBtu
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$1,231
Cost:
$2,782
$1,231 16,416 - - - - $1,231
16,416
kWh
-
-
$
-
-
MMBtu
04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$4,330
Cost:
$17,442
$4,330 57,738 - - - - $4,330
57,738
kWh
-
-
$
-
-
MMBtu
05: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$5,509
Cost:
$14,500
$5,509 73,452 - - - - $5,509
73,452
kWh
-
-
$
-
-
MMBtu
06: 2.6232 INSTALL SET-BACK TIMERS Savings:
$1,433
Cost:
$1,280
$1,433 19,105 - - - - $1,433
19,105
kWh
-
-
$
-
-
MMBtu
07: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES Savings:
$2,268
Cost:
$4,752
$2,268 30,240 - - - - $2,268
30,240
kWh
-
-
$
-
-
MMBtu
08: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$5,900
Cost:
$38,500
- - $5,900 - - - -
-
kWh
$5,900
-
$
-
-
MMBtu
09: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$3,700
Cost:
$1,000
$3,700 49,339 - - - - $3,700
49,339
kWh
-
-
$
-
-
MMBtu
TOTAL RECOMMENDED Savings:
$33,768
Cost:
$104,956
$18,471 246,290 $5,900 - $9,397 2,619 $18,471
246,290
kWh
$5,900
-
$
$9,397
2,619
MMBtu
TOTAL IMPLEMENTED Savings:
$6,364
Cost:
$5,062
$6,364 84,860 - - - - $6,364
84,860
kWh
-
-
$
-
-
MMBtu
Savings
Cost
$ kWh $ $ $ MMBtu
Electricity Usage Electricity Fees Natural Gas Electricity Usage Electricity Fees Natural Gas