Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oregon State University |
---|---|
Assessment Year | 1988 |
Principal Product | POTATOE & CORN CHIPS |
NAICS | n/a |
SIC | 2096 - Potato Chips And Similar Snacks |
Sales | $100,000,000-$500,000,000 |
# of Employees | 470 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 58,000,000 Pounds |
Production Hrs. Annual | 6,864 |
Location (State) | WA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $230,603 | 8,437,866 | kWh | $0.03 |
Natural Gas | $1,242,039 | 261,393 | MMBtu | $4.75 |
TOTAL ENERGY COSTS | $1,472,642 | |||
RECOMMENDED SAVINGS* | $138,093 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $138,093 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $763 Cost: - |
$763 | 28,136 | - | - | - | - |
$763 28,136 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 3.4113 TREAT AND REUSE RINSE WATERS |
Savings: $81,387 Cost: $25,000 |
$(-1,063) | (-39,273) | - | - | $82,450 | - |
$(-1,063) (-39,273) kWh |
- - MMBtu |
$82,450 - $ |
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03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $228 Cost: $150 |
- | - | $228 | 52 | - | - |
- - kWh |
$228 52 MMBtu |
- - $ |
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04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $201 Cost: $349 |
$117 | 4,396 | - | - | $84 | - |
$117 4,396 kWh |
- - MMBtu |
$84 - $ |
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05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $851 Cost: $1,879 |
$1,169 | 43,376 | - | - | $(-318) | - |
$1,169 43,376 kWh |
- - MMBtu |
$(-318) - $ |
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06: 2.2427 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT INCOMING FLUIDS |
Savings: $50,942 Cost: $100,000 |
- | - | $50,942 | 11,710 | - | - |
- - kWh |
$50,942 11,710 MMBtu |
- - $ |
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07: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $3,721 Cost: $21,000 |
- | - | $3,721 | 855 | - | - |
- - kWh |
$3,721 855 MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $138,093 Cost: $148,378 |
$986 | 36,635 | $54,891 | 12,617 | $82,216 | - | $986 36,635 kWh |
$54,891 12,617 MMBtu |
$82,216 - $ |
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TOTAL IMPLEMENTED |
Savings: $138,093 Cost: $148,378 |
$986 | 36,635 | $54,891 | 12,617 | $82,216 | - | $986 36,635 kWh |
$54,891 12,617 MMBtu |
$82,216 - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |