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IAC Assessment: OR0047
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IAC Assessment: OR0047
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IAC Center Oregon State University
Assessment Year 1989
Principal Product FROZEN PRODUCE
NAICS n/a
SIC 2037 - Frozen Fruits And Vegetables
Sales $50,000,000-$100,000,000
# of Employees 150
Plant Area (Sq.Ft.) 0
Annual Production 31,100 Tons
Production Hrs. Annual 5,712
Location (State) OR
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $653,414 14,995,897 kWh $0.04
Natural Gas $76,954 18,978 MMBtu $4.05
TOTAL ENERGY COSTS $730,368
RECOMMENDED SAVINGS* $26,853 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $26,309
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE Savings:
$8,348
Cost:
-
$8,348 189,625 - - - - $8,348
189,625
kWh
-
-
MMBtu
-
-
$
02: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE Savings:
$5,777
Cost:
-
$5,777 131,301 - - - - $5,777
131,301
kWh
-
-
MMBtu
-
-
$
03: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE Savings:
$3,193
Cost:
-
$3,193 72,685 - - - - $3,193
72,685
kWh
-
-
MMBtu
-
-
$
04: 2.6232 INSTALL SET-BACK TIMERS Savings:
$3,718
Cost:
-
$3,041 69,168 - - $677 - $3,041
69,168
kWh
-
-
MMBtu
$677
-
$
05: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$1,679
Cost:
$500
- - $1,679 415 - - -
-
kWh
$1,679
415
MMBtu
-
-
$
06: 2.1213 DIRECT WARMEST AIR TO COMBUSTION INTAKE Savings:
$544
Cost:
$650
- - $544 134 - - -
-
kWh
$544
134
MMBtu
-
-
$
07: 2.2123 INSULATE FEEDWATER TANK Savings:
$435
Cost:
$658
- - $435 107 - - -
-
kWh
$435
107
MMBtu
-
-
$
08: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$3,159
Cost:
$6,810
$3,159 - - - - - $3,159
-
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$26,853
Cost:
$8,618
$23,518 462,779 $2,658 656 $677 - $23,518
462,779
kWh
$2,658
656
MMBtu
$677
-
$
TOTAL IMPLEMENTED Savings:
$26,309
Cost:
$7,968
$23,518 462,779 $2,114 522 $677 - $23,518
462,779
kWh
$2,114
522
MMBtu
$677
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes