IAC logo
IAC Assessment: OR0051
Sponsored by:
DOE MESC
IAC logo
IAC Assessment: OR0051
Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center Oregon State University
Assessment Year 1989
Principal Product MARGARINE AND SHORTENING
NAICS n/a
SIC 2035 - Pickles, Sauces, And Salad Dressings
Sales $5,000,000-$10,000,000
# of Employees 130
Plant Area (Sq.Ft.) 0
Annual Production 60,000,000 Pounds
Production Hrs. Annual 6,000
Location (State) OR
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $237,428 5,385,698 kWh $0.04
Natural Gas $116,983 25,786 MMBtu $4.54
TOTAL ENERGY COSTS $354,411
RECOMMENDED SAVINGS* $49,654 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $42,660
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.6232 INSTALL SET-BACK TIMERS Savings:
$14,990
Cost:
-
$11,889 270,223 - - $3,101 - $11,889
270,223
kWh
-
-
MMBtu
$3,101
-
$
02: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE Savings:
$2,926
Cost:
-
$2,926 66,530 - - - - $2,926
66,530
kWh
-
-
MMBtu
-
-
$
03: 2.2163 USE MINIMUM STEAM OPERATING PRESSURE Savings:
$458
Cost:
-
- - $458 101 - - -
-
kWh
$458
101
MMBtu
-
-
$
04: 2.2111 INSTALL STEAM TRAP Savings:
$23,375
Cost:
$2,335
- - $23,100 5,088 $275 - -
-
kWh
$23,100
5,088
MMBtu
$275
-
$
05: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$444
Cost:
$500
- - $444 123 - - -
-
kWh
$444
123
MMBtu
-
-
$
06: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$467
Cost:
$503
$467 10,551 - - - - $467
10,551
kWh
-
-
MMBtu
-
-
$
07: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE Savings:
$4,450
Cost:
$8,000
$4,450 - - - - - $4,450
-
kWh
-
-
MMBtu
-
-
$
08: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$2,544
Cost:
$5,400
$2,544 - - - - - $2,544
-
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$49,654
Cost:
$16,738
$22,276 347,304 $24,002 5,312 $3,376 - $22,276
347,304
kWh
$24,002
5,312
MMBtu
$3,376
-
$
TOTAL IMPLEMENTED Savings:
$42,660
Cost:
$3,338
$15,282 347,304 $24,002 5,312 $3,376 - $15,282
347,304
kWh
$24,002
5,312
MMBtu
$3,376
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes