Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oregon State University |
---|---|
Assessment Year | 1992 |
Principal Product | CHEESE, BUTTER |
NAICS | n/a |
SIC | 2022 - Cheese, Natural And Processed |
Sales | $5,000,000-$10,000,000 |
# of Employees | 30 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 4,000,000 Pounds |
Production Hrs. Annual | 4,420 |
Location (State) | OR |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $47,357 | 1,072,685 | kWh | $0.04 |
LPG | $63,532 | 9,281 | MMBtu | $6.85 |
TOTAL ENERGY COSTS | $110,889 | |||
RECOMMENDED SAVINGS* | $31,134 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $7,268 |
#|Description |
Savings Cost |
Status | Electricity Usage | LPG | Administrative Changes | Electricity Usage | LPG | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.8118 CHECK FOR ACCURACY OF UTILITY / POWER METERS |
Savings: $23,479 Cost: - |
$23,479 | - | - | - | - | - |
$23,479 - kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.2163 USE MINIMUM STEAM OPERATING PRESSURE |
Savings: $473 Cost: - |
- | - | $473 | 69 | - | - |
- - kWh |
$473 69 MMBtu |
- - $ |
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03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $2,966 Cost: $1,000 |
- | - | $2,966 | 433 | - | - |
- - kWh |
$2,966 433 MMBtu |
- - $ |
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04: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE |
Savings: $200 Cost: - |
$200 | 5,862 | - | - | - | - |
$200 5,862 kWh |
- - MMBtu |
- - $ |
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05: 2.6232 INSTALL SET-BACK TIMERS |
Savings: $387 Cost: $360 |
$228 | 6,448 | - | - | $159 | - |
$228 6,448 kWh |
- - MMBtu |
$159 - $ |
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06: 3.4115 RECOVER AND REUSE COOLING WATER |
Savings: $3,527 Cost: $5,105 |
$(-347) | (-9,965) | $2,952 | 431 | $922 | - |
$(-347) (-9,965) kWh |
$2,952 431 MMBtu |
$922 - $ |
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07: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $102 Cost: $164 |
$102 | 2,052 | - | - | - | - |
$102 2,052 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $31,134 Cost: $6,629 |
$23,662 | 4,397 | $6,391 | 933 | $1,081 | - | $23,662 4,397 kWh |
$6,391 933 MMBtu |
$1,081 - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $7,268 Cost: $6,269 |
$(-45) | (-2,051) | $6,391 | 933 | $922 | - | $(-45) (-2,051) kWh |
$6,391 933 MMBtu |
$922 - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | LPG | Administrative Changes | Electricity Usage | LPG | Administrative Changes |