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IAC Assessment: OR0187
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IAC Assessment: OR0187
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IAC Center Oregon State University
Assessment Year 1993
Principal Product Dimensional Lumber
NAICS n/a
SIC 2421 - Sawmills And Planing Mills, General
Sales $50,000,000-$100,000,000
# of Employees 110
Plant Area (Sq.Ft.) 0
Annual Production 67,000 Thousand Feet
Production Hrs. Annual 8,736
Location (State) OR
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $526,062 12,853,459 kWh $0.04
Natural Gas $375,672 101,883 MMBtu $3.69
TOTAL ENERGY COSTS $901,734
RECOMMENDED SAVINGS* $155,672 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $48,735
#|Description Savings
Cost
Status Electricity Usage Natural Gas Personnel Changes Electricity Usage Natural Gas Personnel Changes
$ kWh $ MMBtu $ $
01: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$10,305
Cost:
$1,800
$10,305 314,478 - - - - $10,305
314,478
kWh
-
-
MMBtu
-
-
$
02: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$5,623
Cost:
$5,500
$5,623 146,249 - - - - $5,623
146,249
kWh
-
-
MMBtu
-
-
$
03: 2.3412 USE WASTE HEAT TO PRODUCE STEAM TO DRIVE A STEAM TURBINE-GENERATOR Savings:
$75,830
Cost:
$146,156
$51,348 1,566,530 $24,482 - - - $51,348
1,566,530
kWh
$24,482
-
MMBtu
-
-
$
04: 2.2511 INSULATE BARE EQUIPMENT Savings:
$1,468
Cost:
$1,287
- - $1,468 398 - - -
-
kWh
$1,468
398
MMBtu
-
-
$
05: 2.4131 SIZE ELECTRIC MOTORS FOR PEAK OPERATING EFFICIENCY Savings:
$29,864
Cost:
$32,720
$29,864 910,903 - - - - $29,864
910,903
kWh
-
-
MMBtu
-
-
$
06: 2.7134 USE PHOTOCELL CONTROLS Savings:
$12,486
Cost:
$4,100
$10,279 251,172 - - $2,207 - $10,279
251,172
kWh
-
-
MMBtu
$2,207
-
$
07: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$2,372
Cost:
-
$2,372 54,220 - - - - $2,372
54,220
kWh
-
-
MMBtu
-
-
$
08: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$1,243
Cost:
$3,171
$1,243 31,653 - - - - $1,243
31,653
kWh
-
-
MMBtu
-
-
$
09: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$2,921
Cost:
$9,700
$2,921 75,615 - - - - $2,921
75,615
kWh
-
-
MMBtu
-
-
$
10: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$13,560
Cost:
$28,500
$13,560 - - - - - $13,560
-
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$155,672
Cost:
$232,934
$127,515 3,350,820 $25,950 398 $2,207 - $127,515
3,350,820
kWh
$25,950
398
MMBtu
$2,207
-
$
TOTAL IMPLEMENTED Savings:
$48,735
Cost:
$50,887
$45,060 841,734 $1,468 398 $2,207 - $45,060
841,734
kWh
$1,468
398
MMBtu
$2,207
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Personnel Changes Electricity Usage Natural Gas Personnel Changes