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IAC Assessment: OR0240
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IAC Assessment: OR0240
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IAC Center Oregon State University
Assessment Year 1995
Principal Product Alder Lumber
NAICS n/a
SIC 2426 - Hardwood Dimension & Flooring Mills
Sales $50,000,000-$100,000,000
# of Employees 200
Plant Area (Sq.Ft.) 169,000
Annual Production 60,000,000 Thousand Feet
Production Hrs. Annual 5,512
Location (State) WA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $612,004 18,391,559 kWh $0.03
Natural Gas $240,750 57,632 MMBtu $4.18
TOTAL ENERGY COSTS $852,754
RECOMMENDED SAVINGS* $92,853 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $59,053
#|Description Savings
Cost
Status Electricity Usage Electricity Usage
$ kWh
01: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$1,950
Cost:
$7,729
$1,950 62,134 $1,950
62,134
kWh
02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$14,925
Cost:
$57,725
$14,925 474,795 $14,925
474,795
kWh
03: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$410
Cost:
-
$410 12,896 $410
12,896
kWh
04: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$38,795
Cost:
$99,195
$38,795 1,203,986 $38,795
1,203,986
kWh
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$18,308
Cost:
$15,000
$18,308 582,649 $18,308
582,649
kWh
06: 2.4224 UPGRADE CONTROLS ON COMPRESSORS Savings:
$2,403
Cost:
$500
$2,403 76,495 $2,403
76,495
kWh
07: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$16,062
Cost:
$20,000
$16,062 - $16,062
-
kWh
TOTAL RECOMMENDED Savings:
$92,853
Cost:
$200,149
$92,853 2,412,955 $92,853
2,412,955
kWh
TOTAL IMPLEMENTED Savings:
$59,053
Cost:
$121,924
$59,053 1,848,769 $59,053
1,848,769
kWh
Savings
Cost
$ kWh
Electricity Usage Electricity Usage