Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oregon State University |
---|---|
Assessment Year | 2004 |
Principal Product | Manufactured Homes |
NAICS | 321992 - Prefabricated Wood Building Manufacturing |
SIC | 2452 - Prefabricated Wood Buildings |
Sales | $10,000,000-$50,000,000 |
# of Employees | 155 |
Plant Area (Sq.Ft.) | 120,000 |
Annual Production | 1,018 Pieces |
Production Hrs. Annual | 2,000 |
Location (State) | WA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $56,953 | 952,270 | kWh | $0.06 |
Electricity Fees | $3,426 | - | $ | - |
Natural Gas | $33,874 | 4,321 | MMBtu | $7.84 |
LPG | $13,597 | 827 | MMBtu | $16.44 |
TOTAL ENERGY COSTS | $197,898 | |||
RECOMMENDED SAVINGS* | $97,370 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $8,930 |
#|Description |
Savings Cost |
Status | Electricity Usage | Personnel Changes | Administrative Changes | Electricity Usage | Personnel Changes | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | $ | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $7,830 Cost: $8,000 |
$7,830 | 124,000 | - | - | - | - |
$7,830 124,000 kWh |
- - $ |
- - $ |
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02: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $1,100 Cost: $2,600 |
$1,100 | 18,200 | - | - | - | - |
$1,100 18,200 kWh |
- - $ |
- - $ |
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03: 4.423 MOVE PRODUCT USING MECHANICAL MEANS |
Savings: $88,440 Cost: $400 |
- | - | $64,800 | - | $23,640 | - |
- - kWh |
$64,800 - $ |
$23,640 - $ |
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TOTAL RECOMMENDED |
Savings: $97,370 Cost: $11,000 |
$8,930 | 142,200 | $64,800 | - | $23,640 | - | $8,930 142,200 kWh |
$64,800 - $ |
$23,640 - $ |
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TOTAL IMPLEMENTED |
Savings: $8,930 Cost: $10,600 |
$8,930 | 142,200 | - | - | - | - | $8,930 142,200 kWh |
- - $ |
- - $ |
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Savings Cost |
$ | kWh | $ | $ | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Personnel Changes | Administrative Changes | Electricity Usage | Personnel Changes | Administrative Changes |