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IAC Assessment: OR0679
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IAC Assessment: OR0679
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IAC Center Oregon State University
Assessment Year 2016
Principal Product Particle Board
NAICS 321219 - Reconstituted Wood Product Manufacturing
SIC 2493 - Reconstituted Wood Products
Sales $100,000,000-$500,000,000
# of Employees 200
Plant Area (Sq.Ft.) 827,640
Annual Production 5,000,000 Units
Production Hrs. Annual 8,736
Location (State) OR
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $4,634,111 70,044,000 kWh $0.07
Natural Gas $1,308,716 426,292 MMBtu $3.07
TOTAL ENERGY COSTS $5,942,827
RECOMMENDED SAVINGS* $202,798 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $143,883
#|Description Savings
Cost
Status Electricity Usage Natural Gas Ancillary Material Cost One-time Revenue or Avoided Cost Electricity Usage Natural Gas Ancillary Material Cost One-time Revenue or Avoided Cost
$ kWh $ MMBtu $ $ $ $
01: 2.6218 TURN OFF EQUIPMENT WHEN NOT IN USE Savings:
$74,285
Cost:
$6,200
$74,285 1,122,803 - - - - - - $74,285
1,122,803
kWh
-
-
MMBtu
-
-
$
-
-
$
02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$20,472
Cost:
-
$20,472 309,426 - - - - - - $20,472
309,426
kWh
-
-
MMBtu
-
-
$
-
-
$
03: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$10,003
Cost:
$10,369
$10,003 151,191 - - - - - - $10,003
151,191
kWh
-
-
MMBtu
-
-
$
-
-
$
04: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$31,513
Cost:
$47,575
- - $31,513 10,265 - - - - -
-
kWh
$31,513
10,265
MMBtu
-
-
$
-
-
$
05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$17,613
Cost:
$47,385
$18,394 278,023 - - $(-1,087) - $306 - $18,394
278,023
kWh
-
-
MMBtu
$(-1,087)
-
$
$306
-
$
06: 2.1224 REPLACE BOILER Savings:
$48,912
Cost:
$250,000
- - $48,912 15,932 - - - - -
-
kWh
$48,912
15,932
MMBtu
-
-
$
-
-
$
TOTAL RECOMMENDED Savings:
$202,798
Cost:
$361,529
$123,154 1,861,443 $80,425 26,197 $(-1,087) - $306 - $123,154
1,861,443
kWh
$80,425
26,197
MMBtu
$(-1,087)
-
$
$306
-
$
TOTAL IMPLEMENTED Savings:
$143,883
Cost:
$101,160
$113,151 1,710,252 $31,513 10,265 $(-1,087) - $306 - $113,151
1,710,252
kWh
$31,513
10,265
MMBtu
$(-1,087)
-
$
$306
-
$
Savings
Cost
$ kWh $ MMBtu $ $ $ $
Electricity Usage Natural Gas Ancillary Material Cost One-time Revenue or Avoided Cost Electricity Usage Natural Gas Ancillary Material Cost One-time Revenue or Avoided Cost