Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oregon State University |
---|---|
Assessment Year | 2016 |
Principal Product | Particle Board |
NAICS | 321219 - Reconstituted Wood Product Manufacturing |
SIC | 2493 - Reconstituted Wood Products |
Sales | $100,000,000-$500,000,000 |
# of Employees | 200 |
Plant Area (Sq.Ft.) | 827,640 |
Annual Production | 5,000,000 Units |
Production Hrs. Annual | 8,736 |
Location (State) | OR |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $4,634,111 | 70,044,000 | kWh | $0.07 |
Natural Gas | $1,308,716 | 426,292 | MMBtu | $3.07 |
TOTAL ENERGY COSTS | $5,942,827 | |||
RECOMMENDED SAVINGS* | $202,798 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $143,883 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Ancillary Material Cost | One-time Revenue or Avoided Cost | Electricity Usage | Natural Gas | Ancillary Material Cost | One-time Revenue or Avoided Cost | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.6218 TURN OFF EQUIPMENT WHEN NOT IN USE |
Savings: $74,285 Cost: $6,200 |
$74,285 | 1,122,803 | - | - | - | - | - | - |
$74,285 1,122,803 kWh |
- - MMBtu |
- - $ |
- - $ |
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02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $20,472 Cost: - |
$20,472 | 309,426 | - | - | - | - | - | - |
$20,472 309,426 kWh |
- - MMBtu |
- - $ |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $10,003 Cost: $10,369 |
$10,003 | 151,191 | - | - | - | - | - | - |
$10,003 151,191 kWh |
- - MMBtu |
- - $ |
- - $ |
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04: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $31,513 Cost: $47,575 |
- | - | $31,513 | 10,265 | - | - | - | - |
- - kWh |
$31,513 10,265 MMBtu |
- - $ |
- - $ |
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05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $17,613 Cost: $47,385 |
$18,394 | 278,023 | - | - | $(-1,087) | - | $306 | - |
$18,394 278,023 kWh |
- - MMBtu |
$(-1,087) - $ |
$306 - $ |
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06: 2.1224 REPLACE BOILER |
Savings: $48,912 Cost: $250,000 |
- | - | $48,912 | 15,932 | - | - | - | - |
- - kWh |
$48,912 15,932 MMBtu |
- - $ |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $202,798 Cost: $361,529 |
$123,154 | 1,861,443 | $80,425 | 26,197 | $(-1,087) | - | $306 | - | $123,154 1,861,443 kWh |
$80,425 26,197 MMBtu |
$(-1,087) - $ |
$306 - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $143,883 Cost: $101,160 |
$113,151 | 1,710,252 | $31,513 | 10,265 | $(-1,087) | - | $306 | - | $113,151 1,710,252 kWh |
$31,513 10,265 MMBtu |
$(-1,087) - $ |
$306 - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Ancillary Material Cost | One-time Revenue or Avoided Cost | Electricity Usage | Natural Gas | Ancillary Material Cost | One-time Revenue or Avoided Cost |