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IAC Assessment: OR0705
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IAC Assessment: OR0705
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Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
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IAC Center Oregon State University
Assessment Year 2018
Principal Product Treated Wastewater
NAICS 221320 - Sewage Treatment Facilities
SIC 4952 - Sewerage Systems
Sales $10,000,000-$50,000,000
# of Employees 80
Plant Area (Sq.Ft.) 2,875,000
Annual Production 59,495,000 Thousand Gallons
Production Hrs. Annual 8,760
Location (State) OR
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $239,426 4,935,600 kWh $0.05
Electricity Demand $97,558 16,632 kW-months/year $5.87
Electricity Fees $32,140 - $ -
Natural Gas $10,326 1,131 MMBtu $9.13
TOTAL ENERGY COSTS $453,796
RECOMMENDED SAVINGS* $1,860,049 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $1,817,773
#|Description Savings
Cost
Status Electricity Usage Electricity Demand Natural Gas Other Gas Electricity Usage Electricity Demand Natural Gas Other Gas
$ kWh $ kW-months/year $ MMBtu $ MMBtu
01: 3.3128 UTILIZE OTHER METHODS TO REMOVE CONTAMINANTS Savings:
$1,817,773
Cost:
$8,000,000
$(-446,439) (-9,203,031) $(-120,994) (-16,154) $(-186,723) (-21,636) $2,571,929 102,877 $(-446,439)
(-9,203,031)
kWh
$(-120,994)
(-16,154)
kW-months/year
$(-186,723)
(-21,636)
MMBtu
$2,571,929
102,877
MMBtu
02: 2.1116 IMPROVE COMBUSTION CONTROL CAPABILITY Savings:
$6,117
Cost:
$13,300
$1,375 28,354 - - $4,742 550 - - $1,375
28,354
kWh
-
-
kW-months/year
$4,742
550
MMBtu
-
-
MMBtu
03: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED Savings:
$1,640
Cost:
$5,820
$1,640 33,803 - - - - - - $1,640
33,803
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
MMBtu
04: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES Savings:
$34,519
Cost:
$150,000
$28,190 581,124 $6,329 796 - - - - $28,190
581,124
kWh
$6,329
796
kW-months/year
-
-
MMBtu
-
-
MMBtu
TOTAL RECOMMENDED Savings:
$1,860,049
Cost:
$8,169,120
$(-415,234) (-8,559,750) $(-114,665) (-15,358) $(-181,981) (-21,086) $2,571,929 102,877 $(-415,234)
(-8,559,750)
kWh
$(-114,665)
(-15,358)
kW-months/year
$(-181,981)
(-21,086)
MMBtu
$2,571,929
102,877
MMBtu
TOTAL IMPLEMENTED Savings:
$1,817,773
Cost:
$8,000,000
$(-446,439) (-9,203,031) $(-120,994) (-16,154) $(-186,723) (-21,636) $2,571,929 102,877 $(-446,439)
(-9,203,031)
kWh
$(-120,994)
(-16,154)
kW-months/year
$(-186,723)
(-21,636)
MMBtu
$2,571,929
102,877
MMBtu
Savings
Cost
$ kWh $ kW-months/year $ MMBtu $ MMBtu
Electricity Usage Electricity Demand Natural Gas Other Gas Electricity Usage Electricity Demand Natural Gas Other Gas