Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oregon State University |
---|---|
Assessment Year | 2018 |
Principal Product | Treated Wastewater |
NAICS | 221320 - Sewage Treatment Facilities |
SIC | 4952 - Sewerage Systems |
Sales | $10,000,000-$50,000,000 |
# of Employees | 80 |
Plant Area (Sq.Ft.) | 2,875,000 |
Annual Production | 59,495,000 Thousand Gallons |
Production Hrs. Annual | 8,760 |
Location (State) | OR |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $239,426 | 4,935,600 | kWh | $0.05 |
Electricity Demand | $97,558 | 16,632 | kW-months/year | $5.87 |
Electricity Fees | $32,140 | - | $ | - |
Natural Gas | $10,326 | 1,131 | MMBtu | $9.13 |
TOTAL ENERGY COSTS | $453,796 | |||
RECOMMENDED SAVINGS* | $1,860,049 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $1,817,773 |
#|Description |
Savings Cost |
Status | Electricity Usage | Electricity Demand | Natural Gas | Other Gas | Electricity Usage | Electricity Demand | Natural Gas | Other Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | kW-months/year | $ | MMBtu | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 3.3128 UTILIZE OTHER METHODS TO REMOVE CONTAMINANTS |
Savings: $1,817,773 Cost: $8,000,000 |
$(-446,439) | (-9,203,031) | $(-120,994) | (-16,154) | $(-186,723) | (-21,636) | $2,571,929 | 102,877 |
$(-446,439) (-9,203,031) kWh |
$(-120,994) (-16,154) kW-months/year |
$(-186,723) (-21,636) MMBtu |
$2,571,929 102,877 MMBtu |
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02: 2.1116 IMPROVE COMBUSTION CONTROL CAPABILITY |
Savings: $6,117 Cost: $13,300 |
$1,375 | 28,354 | - | - | $4,742 | 550 | - | - |
$1,375 28,354 kWh |
- - kW-months/year |
$4,742 550 MMBtu |
- - MMBtu |
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03: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED |
Savings: $1,640 Cost: $5,820 |
$1,640 | 33,803 | - | - | - | - | - | - |
$1,640 33,803 kWh |
- - kW-months/year |
- - MMBtu |
- - MMBtu |
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04: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES |
Savings: $34,519 Cost: $150,000 |
$28,190 | 581,124 | $6,329 | 796 | - | - | - | - |
$28,190 581,124 kWh |
$6,329 796 kW-months/year |
- - MMBtu |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $1,860,049 Cost: $8,169,120 |
$(-415,234) | (-8,559,750) | $(-114,665) | (-15,358) | $(-181,981) | (-21,086) | $2,571,929 | 102,877 | $(-415,234) (-8,559,750) kWh |
$(-114,665) (-15,358) kW-months/year |
$(-181,981) (-21,086) MMBtu |
$2,571,929 102,877 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $1,817,773 Cost: $8,000,000 |
$(-446,439) | (-9,203,031) | $(-120,994) | (-16,154) | $(-186,723) | (-21,636) | $2,571,929 | 102,877 | $(-446,439) (-9,203,031) kWh |
$(-120,994) (-16,154) kW-months/year |
$(-186,723) (-21,636) MMBtu |
$2,571,929 102,877 MMBtu |
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Savings Cost |
$ | kWh | $ | kW-months/year | $ | MMBtu | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Electricity Demand | Natural Gas | Other Gas | Electricity Usage | Electricity Demand | Natural Gas | Other Gas |