Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | San Francisco State University |
---|---|
Assessment Year | 2012 |
Principal Product | Cheese and Whey Products |
NAICS | 311513 - Cheese Manufacturing |
SIC | 2022 - Cheese, Natural And Processed |
Sales | $50,000,000-$100,000,000 |
# of Employees | 98 |
Plant Area (Sq.Ft.) | 53,000 |
Annual Production | 52,000,000 Pounds |
Production Hrs. Annual | 8,616 |
Location (State) | CA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $676,678 | 9,244,000 | kWh | $0.07 |
Electricity Demand | $159,091 | 15,700 | kW-months/year | $10.13 |
Electricity Fees | $15,161 | - | $ | - |
Natural Gas | $361,866 | 60,988 | MMBtu | $5.93 |
TOTAL ENERGY COSTS | $1,212,796 | |||
RECOMMENDED SAVINGS* | $71,870 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $14,554 |
#|Description |
Savings Cost |
Status | Electricity Usage | Electricity Demand | Natural Gas | Personnel Changes | One-time Revenue or Avoided Cost | Electricity Usage | Electricity Demand | Natural Gas | Personnel Changes | One-time Revenue or Avoided Cost | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | kW-months/year | $ | MMBtu | $ | $ | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE |
Savings: $44,715 Cost: - |
$37,718 | 504,255 | $6,997 | 691 | - | - | - | - | - | - |
$37,718 504,255 kWh |
$6,997 691 kW-months/year |
- - MMBtu |
- - $ |
- - $ |
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02: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $7,965 Cost: $672 |
- | - | - | - | $7,965 | 1,343 | - | - | - | - |
- - kWh |
- - kW-months/year |
$7,965 1,343 MMBtu |
- - $ |
- - $ |
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03: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $5,152 Cost: $672 |
$5,152 | 68,876 | - | - | - | - | - | - | - | - |
$5,152 68,876 kWh |
- - kW-months/year |
- - MMBtu |
- - $ |
- - $ |
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04: 2.7224 REDUCE SPACE CONDITIONING DURING NON-WORKING HOURS |
Savings: $3,004 Cost: - |
$640 | 8,559 | - | - | $2,364 | 398 | - | - | - | - |
$640 8,559 kWh |
- - kW-months/year |
$2,364 398 MMBtu |
- - $ |
- - $ |
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05: 2.7292 LOWER CEILING TO REDUCE CONDITIONED SPACE |
Savings: $1,231 Cost: $630 |
$1,231 | 16,454 | - | - | - | - | - | - | - | - |
$1,231 16,454 kWh |
- - kW-months/year |
- - MMBtu |
- - $ |
- - $ |
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06: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $1,437 Cost: $1,299 |
- | - | - | - | $1,437 | 242 | - | - | - | - |
- - kWh |
- - kW-months/year |
$1,437 242 MMBtu |
- - $ |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
07: 2.7132 INSTALL TIMERS ON LIGHT SWITCHES IN LITTLE USED AREAS |
Savings: $326 Cost: $312 |
$283 | 3,796 | $43 | 4 | - | - | - | - | - | - |
$283 3,796 kWh |
$43 4 kW-months/year |
- - MMBtu |
- - $ |
- - $ |
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08: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $8,040 Cost: $28,647 |
$4,548 | 60,808 | $704 | 70 | - | - | $1,506 | - | $1,282 | - |
$4,548 60,808 kWh |
$704 70 kW-months/year |
- - MMBtu |
$1,506 - $ |
$1,282 - $ |
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TOTAL RECOMMENDED |
Savings: $71,870 Cost: $32,232 |
$49,572 | 662,748 | $7,744 | 765 | $11,766 | 1,983 | $1,506 | - | $1,282 | - | $49,572 662,748 kWh |
$7,744 765 kW-months/year |
$11,766 1,983 MMBtu |
$1,506 - $ |
$1,282 - $ |
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TOTAL IMPLEMENTED |
Savings: $14,554 Cost: $2,643 |
$5,152 | 68,876 | - | - | $9,402 | 1,585 | - | - | - | - | $5,152 68,876 kWh |
- - kW-months/year |
$9,402 1,585 MMBtu |
- - $ |
- - $ |
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Savings Cost |
$ | kWh | $ | kW-months/year | $ | MMBtu | $ | $ | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Electricity Demand | Natural Gas | Personnel Changes | One-time Revenue or Avoided Cost | Electricity Usage | Electricity Demand | Natural Gas | Personnel Changes | One-time Revenue or Avoided Cost |