Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Tennessee |
---|---|
Assessment Year | 1987 |
Principal Product | LUNCH MEATS, BACON, HAMS |
NAICS | n/a |
SIC | 2013 - Sausages And Other Prepared Meats |
Sales | $10,000,000-$50,000,000 |
# of Employees | 140 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 16,000,000 Pounds |
Production Hrs. Annual | 8,736 |
Location (State) | TN |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $178,969 | 3,577,960 | kWh | $0.05 |
Natural Gas | $69,775 | 16,540 | MMBtu | $4.22 |
TOTAL ENERGY COSTS | $248,744 | |||
RECOMMENDED SAVINGS* | $24,021 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $20,885 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $12,770 Cost: $2,128 |
- | - | $12,770 | 3,026 | - | - |
- - kWh |
$12,770 3,026 MMBtu |
- - $ |
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02: 2.2163 USE MINIMUM STEAM OPERATING PRESSURE |
Savings: $612 Cost: - |
- | - | $612 | 145 | - | - |
- - kWh |
$612 145 MMBtu |
- - $ |
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03: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $3,136 Cost: $3,000 |
$3,136 | 62,720 | - | - | - | - |
$3,136 62,720 kWh |
- - MMBtu |
- - $ |
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04: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $3,136 Cost: $760 |
$3,136 | 62,720 | - | - | - | - |
$3,136 62,720 kWh |
- - MMBtu |
- - $ |
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05: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $2,271 Cost: $4,080 |
$2,271 | 45,428 | - | - | - | - |
$2,271 45,428 kWh |
- - MMBtu |
- - $ |
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06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $254 Cost: $300 |
- | - | $554 | 132 | $(-300) | - |
- - kWh |
$554 132 MMBtu |
$(-300) - $ |
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07: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT |
Savings: $515 Cost: $800 |
- | - | $515 | 122 | - | - |
- - kWh |
$515 122 MMBtu |
- - $ |
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08: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $1,099 Cost: $150 |
$1,099 | 21,981 | - | - | - | - |
$1,099 21,981 kWh |
- - MMBtu |
- - $ |
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09: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $228 Cost: $72 |
- | - | $228 | 54 | - | - |
- - kWh |
$228 54 MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $24,021 Cost: $11,290 |
$9,642 | 192,849 | $14,679 | 3,479 | $(-300) | - | $9,642 192,849 kWh |
$14,679 3,479 MMBtu |
$(-300) - $ |
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TOTAL IMPLEMENTED |
Savings: $20,885 Cost: $10,530 |
$6,506 | 130,129 | $14,679 | 3,479 | $(-300) | - | $6,506 130,129 kWh |
$14,679 3,479 MMBtu |
$(-300) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |