Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Tennessee |
---|---|
Assessment Year | 1987 |
Principal Product | SAUSAGE LINKS & PATTIES |
NAICS | n/a |
SIC | 2011 - Meat Packing Plants |
Sales | $10,000,000-$50,000,000 |
# of Employees | 75 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 13,000,000 Pounds |
Production Hrs. Annual | 6,240 |
Location (State) | TN |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $97,661 | 1,851,993 | kWh | $0.05 |
LPG | $25,886 | 3,307 | MMBtu | $7.83 |
TOTAL ENERGY COSTS | $123,547 | |||
RECOMMENDED SAVINGS* | $18,178 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $17,961 |
#|Description |
Savings Cost |
Status | Electricity Usage | LPG | Administrative Changes | Electricity Usage | LPG | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $10,904 Cost: $421 |
$3,122 | 58,910 | $7,782 | 990 | - | - |
$3,122 58,910 kWh |
$7,782 990 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.2163 USE MINIMUM STEAM OPERATING PRESSURE |
Savings: $2,633 Cost: - |
- | - | $2,633 | 335 | - | - |
- - kWh |
$2,633 335 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $2,019 Cost: $5,000 |
$2,019 | 38,101 | - | - | - | - |
$2,019 38,101 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
04: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $1,134 Cost: $90 |
$1,134 | 21,395 | - | - | - | - |
$1,134 21,395 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $849 Cost: $75 |
- | - | $849 | 108 | - | - |
- - kWh |
$849 108 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $218 Cost: - |
- | - | $518 | 66 | $(-300) | - |
- - kWh |
$518 66 MMBtu |
$(-300) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
07: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $204 Cost: $50 |
- | - | $204 | 26 | - | - |
- - kWh |
$204 26 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
08: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $217 Cost: - |
$217 | 4,103 | - | - | - | - |
$217 4,103 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $18,178 Cost: $5,636 |
$6,492 | 122,509 | $11,986 | 1,525 | $(-300) | - | $6,492 122,509 kWh |
$11,986 1,525 MMBtu |
$(-300) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $17,961 Cost: $5,636 |
$6,275 | 118,406 | $11,986 | 1,525 | $(-300) | - | $6,275 118,406 kWh |
$11,986 1,525 MMBtu |
$(-300) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | LPG | Administrative Changes | Electricity Usage | LPG | Administrative Changes |