Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Tennessee |
---|---|
Assessment Year | 1988 |
Principal Product | PAINT APPLICATORS |
NAICS | n/a |
SIC | 3991 - Brooms And Brushes |
Sales | $10,000,000-$50,000,000 |
# of Employees | 200 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 24,000,000 Pieces |
Production Hrs. Annual | 7,488 |
Location (State) | TN |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $144,161 | 2,866,940 | kWh | $0.05 |
Natural Gas | $23,991 | 5,417 | MMBtu | $4.43 |
TOTAL ENERGY COSTS | $168,152 | |||
RECOMMENDED SAVINGS* | $17,210 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $16,562 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $6,565 Cost: $415 |
$6,565 | 131,301 | - | - | - | - |
$6,565 131,301 kWh |
- - MMBtu |
- - $ |
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02: 2.7123 KEEP LAMPS AND REFLECTORS CLEAN |
Savings: $6,252 Cost: $14,499 |
$6,199 | 123,974 | - | - | $53 | - |
$6,199 123,974 kWh |
- - MMBtu |
$53 - $ |
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03: 2.7243 IMPROVE AIR CIRCULATION WITH DESTRATIFICATION FANS / OTHER METHODS |
Savings: $135 Cost: $5,000 |
$(-820) | (-16,413) | $955 | 217 | - | - |
$(-820) (-16,413) kWh |
$955 217 MMBtu |
- - $ |
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04: 2.6214 SHUT OFF PILOTS IN STANDBY EQUIPMENT |
Savings: $770 Cost: - |
- | - | $770 | 175 | - | - |
- - kWh |
$770 175 MMBtu |
- - $ |
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05: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $2,491 Cost: - |
$2,491 | 49,824 | - | - | - | - |
$2,491 49,824 kWh |
- - MMBtu |
- - $ |
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06: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $513 Cost: $270 |
$513 | 10,258 | - | - | - | - |
$513 10,258 kWh |
- - MMBtu |
- - $ |
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07: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $484 Cost: $294 |
$484 | 9,672 | - | - | - | - |
$484 9,672 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $17,210 Cost: $20,478 |
$15,432 | 308,616 | $1,725 | 392 | $53 | - | $15,432 308,616 kWh |
$1,725 392 MMBtu |
$53 - $ |
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TOTAL IMPLEMENTED |
Savings: $16,562 Cost: $15,208 |
$15,739 | 314,771 | $770 | 175 | $53 | - | $15,739 314,771 kWh |
$770 175 MMBtu |
$53 - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |