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IAC Assessment: TN0368
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IAC Assessment: TN0368
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Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
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IAC Center University of Tennessee
Assessment Year 1989
Principal Product INDUS. & COMM. LIGHTING
NAICS n/a
SIC 3646 - Commercial Lighting Fixtures
Sales $50,000,000-$100,000,000
# of Employees 290
Plant Area (Sq.Ft.) 0
Annual Production 700,000 Pieces
Production Hrs. Annual 4,420
Location (State) TN
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $236,556 4,306,858 kWh $0.05
Natural Gas $415,249 99,286 MMBtu $4.18
TOTAL ENERGY COSTS $651,805
RECOMMENDED SAVINGS* $42,762 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$5,877
Cost:
-
- - $6,177 1,471 $(-300) - -
-
kWh
$6,177
1,471
MMBtu
$(-300)
-
$
02: 2.2511 INSULATE BARE EQUIPMENT Savings:
$4,310
Cost:
$2,994
- - $4,310 1,264 - - -
-
kWh
$4,310
1,264
MMBtu
-
-
$
03: 2.2441 PREHEAT BOILER MAKEUP WATER WITH WASTE PROCESS HEAT Savings:
$5,212
Cost:
$7,800
- - $5,212 1,241 - - -
-
kWh
$5,212
1,241
MMBtu
-
-
$
04: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES Savings:
$3,470
Cost:
$1,190
- - $3,470 826 - - -
-
kWh
$3,470
826
MMBtu
-
-
$
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$9,946
Cost:
$1,470
$9,946 180,832 - - - - $9,946
180,832
kWh
-
-
MMBtu
-
-
$
06: 2.4324 REPLACE HYDRAULIC / PNEUMATIC EQUIPMENT WITH ELECTRIC EQUIPMENT Savings:
$6,287
Cost:
$25,000
$6,287 114,302 - - - - $6,287
114,302
kWh
-
-
MMBtu
-
-
$
07: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$6,013
Cost:
-
$6,013 109,320 - - - - $6,013
109,320
kWh
-
-
MMBtu
-
-
$
08: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES Savings:
$1,328
Cost:
$450
- - $1,328 316 - - -
-
kWh
$1,328
316
MMBtu
-
-
$
09: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$319
Cost:
$360
- - $319 76 - - -
-
kWh
$319
76
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$42,762
Cost:
$39,264
$22,246 404,454 $20,816 5,194 $(-300) - $22,246
404,454
kWh
$20,816
5,194
MMBtu
$(-300)
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - -
-
kWh
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes