Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Tennessee |
---|---|
Assessment Year | 1990 |
Principal Product | MEN SUITS & SPORT COATS |
NAICS | n/a |
SIC | 2311 - Men's and Boys' Suits, Coats, and Overcoats |
Sales | $50,000,000-$100,000,000 |
# of Employees | 925 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 700,000 Pieces |
Production Hrs. Annual | 3,995 |
Location (State) | KY |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $155,234 | 3,143,904 | kWh | $0.05 |
Natural Gas | $86,111 | 24,048 | MMBtu | $3.58 |
TOTAL ENERGY COSTS | $241,345 | |||
RECOMMENDED SAVINGS* | $21,860 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $9,896 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $2,941 Cost: $500 |
- | - | $2,941 | 817 | - | - |
- - kWh |
$2,941 817 MMBtu |
- - $ |
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02: 2.7123 KEEP LAMPS AND REFLECTORS CLEAN |
Savings: $11,964 Cost: - |
$11,044 | 225,381 | - | - | $920 | - |
$11,044 225,381 kWh |
- - MMBtu |
$920 - $ |
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03: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $2,891 Cost: $1,405 |
- | - | $2,891 | 803 | - | - |
- - kWh |
$2,891 803 MMBtu |
- - $ |
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04: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $1,019 Cost: $3,000 |
- | - | $1,019 | 283 | - | - |
- - kWh |
$1,019 283 MMBtu |
- - $ |
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05: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $810 Cost: - |
- | - | $810 | 225 | - | - |
- - kWh |
$810 225 MMBtu |
- - $ |
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06: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $641 Cost: $200 |
- | - | $641 | 178 | - | - |
- - kWh |
$641 178 MMBtu |
- - $ |
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07: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $862 Cost: $480 |
$862 | 17,585 | - | - | - | - |
$862 17,585 kWh |
- - MMBtu |
- - $ |
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08: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $732 Cost: - |
$732 | 14,947 | - | - | - | - |
$732 14,947 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $21,860 Cost: $5,585 |
$12,638 | 257,913 | $8,302 | 2,306 | $920 | - | $12,638 257,913 kWh |
$8,302 2,306 MMBtu |
$920 - $ |
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TOTAL IMPLEMENTED |
Savings: $9,896 Cost: $5,585 |
$1,594 | 32,532 | $8,302 | 2,306 | - | - | $1,594 32,532 kWh |
$8,302 2,306 MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |