Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Dayton |
---|---|
Assessment Year | 2018 |
Principal Product | Wastewater Treatment |
NAICS | 221320 - Sewage Treatment Facilities |
SIC | 4952 - Sewerage Systems |
Sales | $10,000,000-$50,000,000 |
# of Employees | 45 |
Plant Area (Sq.Ft.) | 609,840 |
Annual Production | 9,100,000 Thousand Gallons |
Production Hrs. Annual | 8,736 |
Location (State) | OH |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $1,436,352 | 15,246,010 | kWh | $0.09 |
Natural Gas | $494,516 | 108,488 | MMBtu | $4.56 |
TOTAL ENERGY COSTS | $1,930,868 | |||
RECOMMENDED SAVINGS* | $325,487 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.6125 KEEP EQUIPMENT CLEAN |
Savings: $25,586 Cost: $12,000 |
- | - | $25,586 | 5,611 |
- - kWh |
$25,586 5,611 MMBtu |
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02: 2.1336 INSTALL EQUIPMENT TO UTILIZE WASTE FUEL |
Savings: $97,475 Cost: $50,000 |
- | - | $97,475 | 21,376 |
- - kWh |
$97,475 21,376 MMBtu |
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03: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $104,092 Cost: $125,000 |
$104,092 | 1,107,360 | - | - |
$104,092 1,107,360 kWh |
- - MMBtu |
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04: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES |
Savings: $30,220 Cost: $126,000 |
$30,220 | 321,492 | - | - |
$30,220 321,492 kWh |
- - MMBtu |
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05: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $18,729 Cost: $13,500 |
$18,729 | 199,249 | - | - |
$18,729 199,249 kWh |
- - MMBtu |
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06: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $18,292 Cost: $8,675 |
$18,292 | 194,597 | - | - |
$18,292 194,597 kWh |
- - MMBtu |
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07: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES |
Savings: $8,160 Cost: $30,000 |
$8,160 | 86,812 | - | - |
$8,160 86,812 kWh |
- - MMBtu |
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08: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $22,933 Cost: $40,500 |
$22,933 | 243,972 | - | - |
$22,933 243,972 kWh |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $325,487 Cost: $405,675 |
$202,426 | 2,153,482 | $123,061 | 26,987 | $202,426 2,153,482 kWh |
$123,061 26,987 MMBtu |
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TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - - kWh |
- - MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |