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IAC Assessment: UD0987
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IAC Assessment: UD0987
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IAC Center University of Dayton
Assessment Year 2018
Principal Product Wastewater Treatment
NAICS 221320 - Sewage Treatment Facilities
SIC 4952 - Sewerage Systems
Sales $10,000,000-$50,000,000
# of Employees 45
Plant Area (Sq.Ft.) 609,840
Annual Production 9,100,000 Thousand Gallons
Production Hrs. Annual 8,736
Location (State) OH
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $1,436,352 15,246,010 kWh $0.09
Natural Gas $494,516 108,488 MMBtu $4.56
TOTAL ENERGY COSTS $1,930,868
RECOMMENDED SAVINGS* $325,487 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Electricity Usage Natural Gas
$ kWh $ MMBtu
01: 2.6125 KEEP EQUIPMENT CLEAN Savings:
$25,586
Cost:
$12,000
- - $25,586 5,611 -
-
kWh
$25,586
5,611
MMBtu
02: 2.1336 INSTALL EQUIPMENT TO UTILIZE WASTE FUEL Savings:
$97,475
Cost:
$50,000
- - $97,475 21,376 -
-
kWh
$97,475
21,376
MMBtu
03: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$104,092
Cost:
$125,000
$104,092 1,107,360 - - $104,092
1,107,360
kWh
-
-
MMBtu
04: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES Savings:
$30,220
Cost:
$126,000
$30,220 321,492 - - $30,220
321,492
kWh
-
-
MMBtu
05: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$18,729
Cost:
$13,500
$18,729 199,249 - - $18,729
199,249
kWh
-
-
MMBtu
06: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$18,292
Cost:
$8,675
$18,292 194,597 - - $18,292
194,597
kWh
-
-
MMBtu
07: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES Savings:
$8,160
Cost:
$30,000
$8,160 86,812 - - $8,160
86,812
kWh
-
-
MMBtu
08: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$22,933
Cost:
$40,500
$22,933 243,972 - - $22,933
243,972
kWh
-
-
MMBtu
TOTAL RECOMMENDED Savings:
$325,487
Cost:
$405,675
$202,426 2,153,482 $123,061 26,987 $202,426
2,153,482
kWh
$123,061
26,987
MMBtu
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - -
-
kWh
-
-
MMBtu
Savings
Cost
$ kWh $ MMBtu
Electricity Usage Natural Gas Electricity Usage Natural Gas