Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Texas A&M, College Station |
---|---|
Assessment Year | 1987 |
Principal Product | INJECTION-MOLDED PLASTIC |
NAICS | n/a |
SIC | 3089 - Plastics Products, Nec |
Sales | $1,000,000-$5,000,000 |
# of Employees | 27 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 3,238,000 Pieces |
Production Hrs. Annual | 5,000 |
Location (State) | TX |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $50,121 | 1,055,979 | kWh | $0.05 |
Natural Gas | $450 | 62 | MMBtu | $7.26 |
TOTAL ENERGY COSTS | $50,571 | |||
RECOMMENDED SAVINGS* | $3,168 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $1,173 |
#|Description |
Savings Cost |
Status | Electricity Usage | Administrative Changes | Electricity Usage | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $367 Cost: $1,070 |
$367 | 11,430 | - | - |
$367 11,430 kWh |
- - $ |
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02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $187 Cost: $53 |
$187 | 3,810 | - | - |
$187 3,810 kWh |
- - $ |
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03: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $204 Cost: $100 |
$204 | 6,155 | - | - |
$204 6,155 kWh |
- - $ |
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04: 3.4154 ELIMINATE LEAKS IN WATER LINES AND VALVES |
Savings: $113 Cost: $100 |
- | - | $113 | - |
- - kWh |
$113 - $ |
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05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $71 Cost: $58 |
$71 | 586 | - | - |
$71 586 kWh |
- - $ |
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06: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $120 Cost: - |
$120 | 3,810 | - | - |
$120 3,810 kWh |
- - $ |
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07: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $111 Cost: - |
$111 | 3,517 | - | - |
$111 3,517 kWh |
- - $ |
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08: 2.3191 USE DEMAND CONTROLLER OR LOAD SHEDDER |
Savings: $1,995 Cost: $2,000 |
$1,995 | - | - | - |
$1,995 - kWh |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $3,168 Cost: $3,381 |
$3,055 | 29,308 | $113 | - | $3,055 29,308 kWh |
$113 - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $1,173 Cost: $1,381 |
$1,060 | 29,308 | $113 | - | $1,060 29,308 kWh |
$113 - $ |
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Savings Cost |
$ | kWh | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Administrative Changes | Electricity Usage | Administrative Changes |