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IAC Assessment: AM0091
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IAC Assessment: AM0091
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IAC Center Texas A&M, College Station
Assessment Year 1990
Principal Product TREATED LUMBER
NAICS n/a
SIC 2491 - Wood Preserving
Sales $10,000,000-$50,000,000
# of Employees 95
Plant Area (Sq.Ft.) 0
Annual Production 1,800 Thousand Feet
Production Hrs. Annual 8,712
Location (State) TX
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $137,743 1,986,811 kWh $0.07
Natural Gas $3,575 968 MMBtu $3.69
Wood $42,720 489,856 MMBtu $0.09
TOTAL ENERGY COSTS $184,038
RECOMMENDED SAVINGS* $36,953 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $13,173
#|Description Savings
Cost
Status Electricity Usage Natural Gas Wood Electricity Usage Natural Gas Wood
$ kWh $ MMBtu $ MMBtu
01: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES Savings:
$12,075
Cost:
$50,000
$12,075 215,416 - - - - $12,075
215,416
kWh
-
-
MMBtu
-
-
MMBtu
02: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$4,720
Cost:
$1,100
$4,720 94,666 - - - - $4,720
94,666
kWh
-
-
MMBtu
-
-
MMBtu
03: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED Savings:
$4,500
Cost:
-
- - - - $4,500 8,345 -
-
kWh
-
-
MMBtu
$4,500
8,345
MMBtu
04: 2.2511 INSULATE BARE EQUIPMENT Savings:
$4,080
Cost:
$16,400
- - - - $4,080 7,560 -
-
kWh
-
-
MMBtu
$4,080
7,560
MMBtu
05: 2.2162 REDUCE EXCESS STEAM BLEEDING Savings:
$3,575
Cost:
$3,750
- - $3,575 1,000 - - -
-
kWh
$3,575
1,000
MMBtu
-
-
MMBtu
06: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$2,030
Cost:
-
$2,030 55,393 - - - - $2,030
55,393
kWh
-
-
MMBtu
-
-
MMBtu
07: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$1,800
Cost:
$3,500
$1,800 - - - - - $1,800
-
kWh
-
-
MMBtu
-
-
MMBtu
08: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS Savings:
$1,600
Cost:
$2,400
- - - - $1,600 3,000 -
-
kWh
-
-
MMBtu
$1,600
3,000
MMBtu
09: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$1,600
Cost:
-
$1,600 32,239 - - - - $1,600
32,239
kWh
-
-
MMBtu
-
-
MMBtu
10: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES Savings:
$602
Cost:
$2,665
- - - - $602 1,115 -
-
kWh
-
-
MMBtu
$602
1,115
MMBtu
11: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$155
Cost:
$319
$155 2,052 - - - - $155
2,052
kWh
-
-
MMBtu
-
-
MMBtu
12: 2.2511 INSULATE BARE EQUIPMENT Savings:
$216
Cost:
$875
- - - - $216 400 -
-
kWh
-
-
MMBtu
$216
400
MMBtu
TOTAL RECOMMENDED Savings:
$36,953
Cost:
$81,009
$22,380 399,766 $3,575 1,000 $10,998 20,420 $22,380
399,766
kWh
$3,575
1,000
MMBtu
$10,998
20,420
MMBtu
TOTAL IMPLEMENTED Savings:
$13,173
Cost:
$27,259
$6,675 96,718 - - $6,498 12,075 $6,675
96,718
kWh
-
-
MMBtu
$6,498
12,075
MMBtu
Savings
Cost
$ kWh $ MMBtu $ MMBtu
Electricity Usage Natural Gas Wood Electricity Usage Natural Gas Wood