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IAC Assessment: AM0092
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IAC Assessment: AM0092
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IAC Center Texas A&M, College Station
Assessment Year 1990
Principal Product FROZEN YOGURT MIXTURE
NAICS n/a
SIC 2023 - Dry, Condensed, Evaporated Products
Sales $100,000,000-$500,000,000
# of Employees 178
Plant Area (Sq.Ft.) 0
Annual Production 16,000 Thousand Gallons
Production Hrs. Annual 4,256
Location (State) TX
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $660,398 16,060,962 kWh $0.04
Natural Gas $76,422 17,858 MMBtu $4.28
TOTAL ENERGY COSTS $736,820
RECOMMENDED SAVINGS* $13,370 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $8,372
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.4321 UPGRADE OBSOLETE EQUIPMENT Savings:
$5,963
Cost:
-
$5,963 201,348 - - - - $5,963
201,348
kWh
-
-
MMBtu
-
-
$
02: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$2,950
Cost:
$7,000
- - $2,950 690 - - -
-
kWh
$2,950
690
MMBtu
-
-
$
03: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED Savings:
$1,610
Cost:
$30
- - - - $1,610 - -
-
kWh
-
-
MMBtu
$1,610
-
$
04: 2.7133 USE SEPARATE SWITCHES ON PERIMETER LIGHTING WHICH MAY BE TURNED OFF WHEN NATURAL LIGHT IS AVAILABLE Savings:
$1,153
Cost:
$2,300
$1,153 38,980 - - - - $1,153
38,980
kWh
-
-
MMBtu
-
-
$
05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$225
Cost:
$49
$225 3,517 - - - - $225
3,517
kWh
-
-
MMBtu
-
-
$
06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$895
Cost:
$3,850
$350 8,792 - - $545 - $350
8,792
kWh
-
-
MMBtu
$545
-
$
07: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES Savings:
$431
Cost:
$860
- - $431 80 - - -
-
kWh
$431
80
MMBtu
-
-
$
08: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$143
Cost:
$14
$143 3,517 - - - - $143
3,517
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$13,370
Cost:
$14,103
$7,834 256,154 $3,381 770 $2,155 - $7,834
256,154
kWh
$3,381
770
MMBtu
$2,155
-
$
TOTAL IMPLEMENTED Savings:
$8,372
Cost:
$953
$6,331 208,382 $431 80 $1,610 - $6,331
208,382
kWh
$431
80
MMBtu
$1,610
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes