Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Texas A&M, College Station |
---|---|
Assessment Year | 1991 |
Principal Product | HARDWOOD LUMBER |
NAICS | n/a |
SIC | 2421 - Sawmills And Planing Mills, General |
Sales | $10,000,000-$50,000,000 |
# of Employees | 34 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 10,000 Thousand Feet |
Production Hrs. Annual | 8,736 |
Location (State) | TX |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $100,991 | 2,068,288 | kWh | $0.05 |
Wood | $55,579 | 90,200 | MMBtu | $0.62 |
TOTAL ENERGY COSTS | $156,570 | |||
RECOMMENDED SAVINGS* | $5,274 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $4,771 |
#|Description |
Savings Cost |
Status | Electricity Usage | Wood | Administrative Changes | Electricity Usage | Wood | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $1,156 Cost: $748 |
$1,156 | 31,360 | - | - | - | - |
$1,156 31,360 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.7221 LOWER TEMPERATURE DURING THE WINTER SEASON AND VICE-VERSA |
Savings: $1,500 Cost: - |
$1,500 | 14,654 | - | - | - | - |
$1,500 14,654 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $1,350 Cost: - |
$1,350 | 37,808 | - | - | - | - |
$1,350 37,808 kWh |
- - MMBtu |
- - $ |
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04: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $540 Cost: $1,270 |
- | - | $540 | 880 | - | - |
- - kWh |
$540 880 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE |
Savings: $503 Cost: - |
- | - | - | - | $503 | - |
- - kWh |
- - MMBtu |
$503 - $ |
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06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $55 Cost: $14 |
$55 | 586 | - | - | - | - |
$55 586 kWh |
- - MMBtu |
- - $ |
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07: 2.6232 INSTALL SET-BACK TIMERS |
Savings: $170 Cost: - |
$170 | 5,569 | - | - | - | - |
$170 5,569 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $5,274 Cost: $2,032 |
$4,231 | 89,977 | $540 | 880 | $503 | - | $4,231 89,977 kWh |
$540 880 MMBtu |
$503 - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $4,771 Cost: $2,032 |
$4,231 | 89,977 | $540 | 880 | - | - | $4,231 89,977 kWh |
$540 880 MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Wood | Administrative Changes | Electricity Usage | Wood | Administrative Changes |