Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Arizona State University |
---|---|
Assessment Year | 1991 |
Principal Product | OAK BEDROOM FURNITURE |
NAICS | n/a |
SIC | 2511 - Wood Household Furniture |
Sales | $10,000,000-$50,000,000 |
# of Employees | 75 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 0 Units |
Production Hrs. Annual | 2,100 |
Location (State) | AZ |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $104,307 | 1,233,001 | kWh | $0.08 |
TOTAL ENERGY COSTS | $104,307 | |||
RECOMMENDED SAVINGS* | $14,664 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $14,664 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT |
Savings: $11,610 Cost: - |
$36,449 | 430,832 | $(-22,089) | (-4,909) | $(-2,750) | - |
$36,449 430,832 kWh |
$(-22,089) (-4,909) MMBtu |
$(-2,750) - $ |
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02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $95 Cost: $155 |
$95 | 1,172 | - | - | - | - |
$95 1,172 kWh |
- - MMBtu |
- - $ |
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03: 2.6232 INSTALL SET-BACK TIMERS |
Savings: $140 Cost: $150 |
$140 | 1,758 | - | - | - | - |
$140 1,758 kWh |
- - MMBtu |
- - $ |
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04: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $402 Cost: $200 |
$402 | 4,689 | - | - | - | - |
$402 4,689 kWh |
- - MMBtu |
- - $ |
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05: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $390 Cost: $1,560 |
$390 | 4,689 | - | - | - | - |
$390 4,689 kWh |
- - MMBtu |
- - $ |
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06: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $696 Cost: $500 |
$696 | 8,206 | - | - | - | - |
$696 8,206 kWh |
- - MMBtu |
- - $ |
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07: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $1,331 Cost: $1,100 |
$1,331 | 15,826 | - | - | - | - |
$1,331 15,826 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $14,664 Cost: $3,665 |
$39,503 | 467,172 | $(-22,089) | (-4,909) | $(-2,750) | - | $39,503 467,172 kWh |
$(-22,089) (-4,909) MMBtu |
$(-2,750) - $ |
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TOTAL IMPLEMENTED |
Savings: $14,664 Cost: $3,665 |
$39,503 | 467,172 | $(-22,089) | (-4,909) | $(-2,750) | - | $39,503 467,172 kWh |
$(-22,089) (-4,909) MMBtu |
$(-2,750) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |