Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Arizona State University |
---|---|
Assessment Year | 1992 |
Principal Product | ICE CREAM/ NOVELTY ITEMS |
NAICS | n/a |
SIC | 2024 - Ice Cream And Frozen Desserts |
Sales | $10,000,000-$50,000,000 |
# of Employees | 70 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 5,500 Thousand Gallons |
Production Hrs. Annual | 4,160 |
Location (State) | AZ |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $476,182 | 6,844,959 | kWh | $0.07 |
TOTAL ENERGY COSTS | $476,182 | |||
RECOMMENDED SAVINGS* | $67,357 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.3415 USE A FOSSIL FUEL ENGINE TO COGENERATE ELECTRICITY OR MOTIVE POWER; AND UTILIZE HEAT |
Savings: $41,691 Cost: $235,000 |
$122,422 | 1,759,672 | $(-54,336) | (-18,499) | $(-26,395) | - |
$122,422 1,759,672 kWh |
$(-54,336) (-18,499) MMBtu |
$(-26,395) - $ |
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02: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $6,343 Cost: - |
$6,343 | 91,149 | - | - | - | - |
$6,343 91,149 kWh |
- - MMBtu |
- - $ |
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03: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $3,703 Cost: $18,211 |
$3,703 | 53,341 | - | - | - | - |
$3,703 53,341 kWh |
- - MMBtu |
- - $ |
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04: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $2,613 Cost: - |
$2,613 | 37,515 | - | - | - | - |
$2,613 37,515 kWh |
- - MMBtu |
- - $ |
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05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $3,028 Cost: $300 |
$3,028 | 43,669 | - | - | - | - |
$3,028 43,669 kWh |
- - MMBtu |
- - $ |
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06: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $2,000 Cost: $3,276 |
$2,000 | 28,722 | - | - | - | - |
$2,000 28,722 kWh |
- - MMBtu |
- - $ |
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07: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $1,215 Cost: $3,210 |
$1,290 | 18,464 | - | - | $(-75) | - |
$1,290 18,464 kWh |
- - MMBtu |
$(-75) - $ |
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08: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $989 Cost: $200 |
- | - | $989 | 220 | - | - |
- - kWh |
$989 220 MMBtu |
- - $ |
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09: 3.4156 USE FLOW CONTROL VALVES ON EQUIPMENT TO OPTIMIZE WATER USE |
Savings: $5,775 Cost: $6,535 |
- | - | - | - | $5,775 | - |
- - kWh |
- - MMBtu |
$5,775 - $ |
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TOTAL RECOMMENDED |
Savings: $67,357 Cost: $266,732 |
$141,399 | 2,032,532 | $(-53,347) | (-18,279) | $(-20,695) | - | $141,399 2,032,532 kWh |
$(-53,347) (-18,279) MMBtu |
$(-20,695) - $ |
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TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - | - | - - kWh |
- - MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |