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IAC Assessment: AS0057
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IAC Assessment: AS0057
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IAC Center Arizona State University
Assessment Year 1992
Principal Product ICE CREAM/ NOVELTY ITEMS
NAICS n/a
SIC 2024 - Ice Cream And Frozen Desserts
Sales $10,000,000-$50,000,000
# of Employees 70
Plant Area (Sq.Ft.) 0
Annual Production 5,500 Thousand Gallons
Production Hrs. Annual 4,160
Location (State) AZ
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $476,182 6,844,959 kWh $0.07
TOTAL ENERGY COSTS $476,182
RECOMMENDED SAVINGS* $67,357 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.3415 USE A FOSSIL FUEL ENGINE TO COGENERATE ELECTRICITY OR MOTIVE POWER; AND UTILIZE HEAT Savings:
$41,691
Cost:
$235,000
$122,422 1,759,672 $(-54,336) (-18,499) $(-26,395) - $122,422
1,759,672
kWh
$(-54,336)
(-18,499)
MMBtu
$(-26,395)
-
$
02: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$6,343
Cost:
-
$6,343 91,149 - - - - $6,343
91,149
kWh
-
-
MMBtu
-
-
$
03: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$3,703
Cost:
$18,211
$3,703 53,341 - - - - $3,703
53,341
kWh
-
-
MMBtu
-
-
$
04: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$2,613
Cost:
-
$2,613 37,515 - - - - $2,613
37,515
kWh
-
-
MMBtu
-
-
$
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$3,028
Cost:
$300
$3,028 43,669 - - - - $3,028
43,669
kWh
-
-
MMBtu
-
-
$
06: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$2,000
Cost:
$3,276
$2,000 28,722 - - - - $2,000
28,722
kWh
-
-
MMBtu
-
-
$
07: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$1,215
Cost:
$3,210
$1,290 18,464 - - $(-75) - $1,290
18,464
kWh
-
-
MMBtu
$(-75)
-
$
08: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES Savings:
$989
Cost:
$200
- - $989 220 - - -
-
kWh
$989
220
MMBtu
-
-
$
09: 3.4156 USE FLOW CONTROL VALVES ON EQUIPMENT TO OPTIMIZE WATER USE Savings:
$5,775
Cost:
$6,535
- - - - $5,775 - -
-
kWh
-
-
MMBtu
$5,775
-
$
TOTAL RECOMMENDED Savings:
$67,357
Cost:
$266,732
$141,399 2,032,532 $(-53,347) (-18,279) $(-20,695) - $141,399
2,032,532
kWh
$(-53,347)
(-18,279)
MMBtu
$(-20,695)
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - -
-
kWh
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes