Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Arizona State University |
---|---|
Assessment Year | 1992 |
Principal Product | PHARMACEUTICAL DRUGS |
NAICS | n/a |
SIC | 2834 - Pharmaceutical Preparations |
Sales | $100,000,000-$500,000,000 |
# of Employees | 500 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 500,000 Pieces |
Production Hrs. Annual | 5,304 |
Location (State) | AZ |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $822,354 | 13,906,800 | kWh | $0.06 |
TOTAL ENERGY COSTS | $822,354 | |||
RECOMMENDED SAVINGS* | $303,419 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $303,419 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $793 Cost: $6,684 |
$793 | 13,482 | - | - | - | - |
$793 13,482 kWh |
- - MMBtu |
- - $ |
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02: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $2,648 Cost: $6,290 |
$2,648 | 44,842 | - | - | - | - |
$2,648 44,842 kWh |
- - MMBtu |
- - $ |
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03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $22,425 Cost: $82,095 |
$22,425 | 379,250 | - | - | - | - |
$22,425 379,250 kWh |
- - MMBtu |
- - $ |
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04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $352 Cost: $1,008 |
$352 | 5,862 | - | - | - | - |
$352 5,862 kWh |
- - MMBtu |
- - $ |
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05: 2.3415 USE A FOSSIL FUEL ENGINE TO COGENERATE ELECTRICITY OR MOTIVE POWER; AND UTILIZE HEAT |
Savings: $264,625 Cost: $2,031,000 |
$624,765 | 10,772,568 | $(-198,551) | (-72,462) | $(-161,589) | - |
$624,765 10,772,568 kWh |
$(-198,551) (-72,462) MMBtu |
$(-161,589) - $ |
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06: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $264 Cost: $280 |
- | - | $264 | 58 | - | - |
- - kWh |
$264 58 MMBtu |
- - $ |
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07: 2.1243 USE HEAT FROM BOILER BLOWDOWN TO PREHEAT BOILER FEED WATER |
Savings: $2,838 Cost: $7,000 |
- | - | $2,838 | 621 | - | - |
- - kWh |
$2,838 621 MMBtu |
- - $ |
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08: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $6,956 Cost: $19,000 |
- | - | $6,956 | 1,522 | - | - |
- - kWh |
$6,956 1,522 MMBtu |
- - $ |
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09: 2.1242 MINIMIZE BOILER BLOWDOWN WITH BETTER FEEDWATER TREATMENT |
Savings: $2,518 Cost: $5,000 |
- | - | $2,518 | 531 | - | - |
- - kWh |
$2,518 531 MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $303,419 Cost: $2,158,357 |
$650,983 | 11,216,004 | $(-185,975) | (-69,730) | $(-161,589) | - | $650,983 11,216,004 kWh |
$(-185,975) (-69,730) MMBtu |
$(-161,589) - $ |
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TOTAL IMPLEMENTED |
Savings: $303,419 Cost: $2,158,357 |
$650,983 | 11,216,004 | $(-185,975) | (-69,730) | $(-161,589) | - | $650,983 11,216,004 kWh |
$(-185,975) (-69,730) MMBtu |
$(-161,589) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |