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IAC Assessment: AS0097
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IAC Assessment: AS0097
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IAC Center Arizona State University
Assessment Year 1993
Principal Product POWDERED LAXATIVES
NAICS n/a
SIC 2834 - Pharmaceutical Preparations
Sales $50,000,000-$100,000,000
# of Employees 250
Plant Area (Sq.Ft.) 0
Annual Production 2,900,000 Pieces
Production Hrs. Annual 6,240
Location (State) AZ
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $866,894 11,343,494 kWh $0.08
Natural Gas $117,448 27,285 MMBtu $4.30
TOTAL ENERGY COSTS $984,342
RECOMMENDED SAVINGS* $227,666 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $62,736
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$7,381
Cost:
$9,500
- - $7,381 1,717 - - -
-
kWh
$7,381
1,717
MMBtu
-
-
$
02: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$5,546
Cost:
$2,000
- - $5,546 1,290 - - -
-
kWh
$5,546
1,290
MMBtu
-
-
$
03: 2.3415 USE A FOSSIL FUEL ENGINE TO COGENERATE ELECTRICITY OR MOTIVE POWER; AND UTILIZE HEAT Savings:
$108,898
Cost:
$235,000
$100,245 1,466,295 $(-13,343) (-7,266) $21,996 - $100,245
1,466,295
kWh
$(-13,343)
(-7,266)
MMBtu
$21,996
-
$
04: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE Savings:
$61,773
Cost:
$50,500
$61,773 - - - - - $61,773
-
kWh
-
-
MMBtu
-
-
$
05: 2.7252 UTILIZE AN EVAPORATIVE AIR PRE-COOLER OR OTHER HEAT EXCHANGER IN AC SYSTEM Savings:
$9,095
Cost:
$35,400
$9,095 118,992 - - - - $9,095
118,992
kWh
-
-
MMBtu
-
-
$
06: 2.2622 REPLACE EXISTING CHILLER WITH HIGH EFFICIENCY MODEL Savings:
$23,277
Cost:
$88,239
$23,277 304,807 - - - - $23,277
304,807
kWh
-
-
MMBtu
-
-
$
07: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$822
Cost:
$800
$822 10,844 - - - - $822
10,844
kWh
-
-
MMBtu
-
-
$
08: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$7,582
Cost:
-
$7,582 99,355 - - - - $7,582
99,355
kWh
-
-
MMBtu
-
-
$
09: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$141
Cost:
$180
$141 1,758 - - - - $141
1,758
kWh
-
-
MMBtu
-
-
$
10: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT Savings:
$3,151
Cost:
$5,265
$3,762 49,238 $(-611) (-142) - - $3,762
49,238
kWh
$(-611)
(-142)
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$227,666
Cost:
$426,884
$206,697 2,051,289 $(-1,027) (-4,401) $21,996 - $206,697
2,051,289
kWh
$(-1,027)
(-4,401)
MMBtu
$21,996
-
$
TOTAL IMPLEMENTED Savings:
$62,736
Cost:
$51,480
$62,736 12,602 - - - - $62,736
12,602
kWh
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes