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IAC Assessment: CO0021
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IAC Assessment: CO0021
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IAC Center Colorado State University
Assessment Year 1985
Principal Product WIRE BELTS & CHAINS
NAICS n/a
SIC 3496 - Misc. Fabricated Wire Products
Sales $1,000,000-$5,000,000
# of Employees 75
Plant Area (Sq.Ft.) 0
Annual Production 5,000,000 Pieces
Production Hrs. Annual 2,470
Location (State) CO
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $98,841 718,933 kWh $0.14
Natural Gas $59,963 12,636 MMBtu $4.75
TOTAL ENERGY COSTS $158,804
RECOMMENDED SAVINGS* $9,956 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $6,049
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$474
Cost:
$219
$474 7,327 - - - - $474
7,327
kWh
-
-
MMBtu
-
-
$
02: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$440
Cost:
$500
- - $440 93 - - -
-
kWh
$440
93
MMBtu
-
-
$
03: 2.2511 INSULATE BARE EQUIPMENT Savings:
$811
Cost:
$200
- - $811 171 - - -
-
kWh
$811
171
MMBtu
-
-
$
04: 2.2511 INSULATE BARE EQUIPMENT Savings:
$149
Cost:
$200
- - $149 31 - - -
-
kWh
$149
31
MMBtu
-
-
$
05: 2.3134 SHIFT FROM DAYTIME TO NIGHTTIME OPERATION Savings:
$2,675
Cost:
-
$7,675 - - - $(-5,000) - $7,675
-
kWh
-
-
MMBtu
$(-5,000)
-
$
06: 2.3521 REDUCE LOAD ON ELECTRICAL CONDUCTOR TO REDUCE HEATING LOSSES Savings:
$3,907
Cost:
$1,000
$3,907 61,254 - - - - $3,907
61,254
kWh
-
-
MMBtu
-
-
$
07: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES Savings:
$532
Cost:
$500
- - $532 112 - - -
-
kWh
$532
112
MMBtu
-
-
$
08: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$327
Cost:
$50
$327 5,275 - - - - $327
5,275
kWh
-
-
MMBtu
-
-
$
09: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS Savings:
$174
Cost:
$100
$174 2,638 - - - - $174
2,638
kWh
-
-
MMBtu
-
-
$
10: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME Savings:
$467
Cost:
$100
$467 7,327 - - - - $467
7,327
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$9,956
Cost:
$2,869
$13,024 83,821 $1,932 407 $(-5,000) - $13,024
83,821
kWh
$1,932
407
MMBtu
$(-5,000)
-
$
TOTAL IMPLEMENTED Savings:
$6,049
Cost:
$1,869
$9,117 22,567 $1,932 407 $(-5,000) - $9,117
22,567
kWh
$1,932
407
MMBtu
$(-5,000)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes