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IAC Assessment: GT0151
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IAC Assessment: GT0151
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IAC Center Georgia Institute of Technology
Assessment Year 1982
Principal Product SYNTHETIC CARPET YARNS
NAICS n/a
SIC 2281 - Yarn Spinning Mills
Sales $10,000,000-$50,000,000
# of Employees 450
Plant Area (Sq.Ft.) 0
Annual Production 16,600,000 Pounds
Production Hrs. Annual 7,200
Location (State) GA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $624,973 16,742,966 kWh $0.04
Natural Gas $247,675 75,976 MMBtu $3.26
Fuel Oil #6 $92,212 17,738 MMBtu $5.20
TOTAL ENERGY COSTS $964,860
RECOMMENDED SAVINGS* $138,012 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $62,689
#|Description Savings
Cost
Status Electricity Usage Natural Gas Fuel Oil #6 Electricity Usage Natural Gas Fuel Oil #6
$ kWh $ MMBtu $ MMBtu
01: 2.7226 USE COMPUTER PROGRAMS TO OPTIMIZE HVAC PERFORMANCE Savings:
$14,476
Cost:
$20,520
$14,476 650,938 - - - - $14,476
650,938
kWh
-
-
MMBtu
-
-
MMBtu
02: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS Savings:
$42,062
Cost:
-
$42,062 1,127,784 - - - - $42,062
1,127,784
kWh
-
-
MMBtu
-
-
MMBtu
03: 2.1232 KEEP BOILER TUBES CLEAN Savings:
$20,627
Cost:
$500
- - $15,025 4,615 $5,602 1,064 -
-
kWh
$15,025
4,615
MMBtu
$5,602
1,064
MMBtu
04: 2.5123 REDUCE FLUID FLOW RATES Savings:
$6,797
Cost:
$5,000
- - $6,797 1,570 - - -
-
kWh
$6,797
1,570
MMBtu
-
-
MMBtu
05: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$40,030
Cost:
$29,973
$40,030 1,082,063 - - - - $40,030
1,082,063
kWh
-
-
MMBtu
-
-
MMBtu
06: 2.3191 USE DEMAND CONTROLLER OR LOAD SHEDDER Savings:
$13,374
Cost:
$9,000
$13,374 - - - - - $13,374
-
kWh
-
-
MMBtu
-
-
MMBtu
07: 2.2511 INSULATE BARE EQUIPMENT Savings:
$646
Cost:
$1,609
$646 17,292 - - - - $646
17,292
kWh
-
-
MMBtu
-
-
MMBtu
TOTAL RECOMMENDED Savings:
$138,012
Cost:
$66,602
$110,588 2,878,077 $21,822 6,185 $5,602 1,064 $110,588
2,878,077
kWh
$21,822
6,185
MMBtu
$5,602
1,064
MMBtu
TOTAL IMPLEMENTED Savings:
$62,689
Cost:
$500
$42,062 1,127,784 $15,025 4,615 $5,602 1,064 $42,062
1,127,784
kWh
$15,025
4,615
MMBtu
$5,602
1,064
MMBtu
Savings
Cost
$ kWh $ MMBtu $ MMBtu
Electricity Usage Natural Gas Fuel Oil #6 Electricity Usage Natural Gas Fuel Oil #6