Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
---|---|
Assessment Year | 1983 |
Principal Product | DEBONED CHICKEN |
NAICS | n/a |
SIC | 2015 - Poultry Slaughtering And Processing |
Sales | $10,000,000-$50,000,000 |
# of Employees | 54 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 52,000,000 Pounds |
Production Hrs. Annual | 3,120 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $163,941 | 3,028,136 | kWh | $0.05 |
Natural Gas | $20,550 | 4,584 | MMBtu | $4.48 |
TOTAL ENERGY COSTS | $184,491 | |||
RECOMMENDED SAVINGS* | $12,860 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $11,771 Cost: $49,000 |
$11,771 | 217,761 | - | - |
$11,771 217,761 kWh |
- - MMBtu |
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02: 2.2523 REDUCE INFILTRATION TO REFRIGERATED AREAS; ISOLATE HOT EQUIPMENT FROM REFRIGERATED AREAS |
Savings: $382 Cost: $200 |
$382 | 7,034 | - | - |
$382 7,034 kWh |
- - MMBtu |
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03: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $334 Cost: $100 |
- | - | $334 | 77 |
- - kWh |
$334 77 MMBtu |
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04: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $225 Cost: $133 |
- | - | $225 | 44 |
- - kWh |
$225 44 MMBtu |
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05: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $148 Cost: $85 |
- | - | $148 | 29 |
- - kWh |
$148 29 MMBtu |
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TOTAL RECOMMENDED |
Savings: $12,860 Cost: $49,518 |
$12,153 | 224,795 | $707 | 150 | $12,153 224,795 kWh |
$707 150 MMBtu |
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TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - - kWh |
- - MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |