Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
---|---|
Assessment Year | 1991 |
Principal Product | COTTON HOSIERY |
NAICS | n/a |
SIC | 2252 - Hosiery, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 350 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 3,000,000 Pieces |
Production Hrs. Annual | 4,500 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $213,128 | 2,517,292 | kWh | $0.08 |
Natural Gas | $170,171 | 32,618 | MMBtu | $5.22 |
TOTAL ENERGY COSTS | $383,299 | |||
RECOMMENDED SAVINGS* | $44,663 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $44,663 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $5,535 Cost: $1,000 |
$5,535 | 65,358 | - | - |
$5,535 65,358 kWh |
- - MMBtu |
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02: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $553 Cost: $2,462 |
$553 | 6,448 | - | - |
$553 6,448 kWh |
- - MMBtu |
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03: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $225 Cost: $800 |
$225 | 2,638 | - | - |
$225 2,638 kWh |
- - MMBtu |
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04: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $1,810 Cost: $1,000 |
$1,810 | 21,395 | - | - |
$1,810 21,395 kWh |
- - MMBtu |
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05: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED |
Savings: $1,900 Cost: $500 |
$1,900 | 22,567 | - | - |
$1,900 22,567 kWh |
- - MMBtu |
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06: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $6,770 Cost: $1,990 |
- | - | $6,770 | 1,298 |
- - kWh |
$6,770 1,298 MMBtu |
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07: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $1,390 Cost: $1,000 |
- | - | $1,390 | 266 |
- - kWh |
$1,390 266 MMBtu |
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08: 2.2449 RECOVER HEAT FROM EXHAUSTED STEAM, HOT AIR OR HOT WATER |
Savings: $24,470 Cost: $53,000 |
- | - | $24,470 | 4,688 |
- - kWh |
$24,470 4,688 MMBtu |
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09: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES |
Savings: $2,010 Cost: $6,240 |
- | - | $2,010 | 385 |
- - kWh |
$2,010 385 MMBtu |
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TOTAL RECOMMENDED |
Savings: $44,663 Cost: $67,992 |
$10,023 | 118,406 | $34,640 | 6,637 | $10,023 118,406 kWh |
$34,640 6,637 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $44,663 Cost: $67,992 |
$10,023 | 118,406 | $34,640 | 6,637 | $10,023 118,406 kWh |
$34,640 6,637 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |