Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
---|---|
Assessment Year | 1991 |
Principal Product | SNACK CHIPS |
NAICS | n/a |
SIC | 2096 - Potato Chips And Similar Snacks |
Sales | $10,000,000-$50,000,000 |
# of Employees | 250 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 23,000,000 Pounds |
Production Hrs. Annual | 8,736 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $432,766 | 8,156,507 | kWh | $0.05 |
Natural Gas | $273,380 | 87,795 | MMBtu | $3.11 |
TOTAL ENERGY COSTS | $706,146 | |||
RECOMMENDED SAVINGS* | $28,127 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $9,380 Cost: - |
- | - | $9,980 | 3,210 | $(-600) | - |
- - kWh |
$9,980 3,210 MMBtu |
$(-600) - $ |
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02: 3.4154 ELIMINATE LEAKS IN WATER LINES AND VALVES |
Savings: $902 Cost: - |
- | - | $902 | 290 | - | - |
- - kWh |
$902 290 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED |
Savings: $10,480 Cost: $3,670 |
- | - | $10,480 | 3,370 | - | - |
- - kWh |
$10,480 3,370 MMBtu |
- - $ |
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04: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $2,450 Cost: $425 |
- | - | $2,450 | 720 | - | - |
- - kWh |
$2,450 720 MMBtu |
- - $ |
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05: 2.2427 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT INCOMING FLUIDS |
Savings: $1,030 Cost: $4,500 |
- | - | $1,030 | 330 | - | - |
- - kWh |
$1,030 330 MMBtu |
- - $ |
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06: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $2,350 Cost: $2,570 |
$2,350 | 135,991 | - | - | - | - |
$2,350 135,991 kWh |
- - MMBtu |
- - $ |
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07: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $1,535 Cost: - |
- | - | $1,835 | 590 | $(-300) | - |
- - kWh |
$1,835 590 MMBtu |
$(-300) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $28,127 Cost: $11,165 |
$2,350 | 135,991 | $26,677 | 8,510 | $(-900) | - | $2,350 135,991 kWh |
$26,677 8,510 MMBtu |
$(-900) - $ |
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TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - | - | - - kWh |
- - MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |