Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
---|---|
Assessment Year | 1992 |
Principal Product | RUBBER AUTO PARTS |
NAICS | n/a |
SIC | 3069 - Fabricated Rubber Products, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 240 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 6,500,000 Pounds |
Production Hrs. Annual | 6,000 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $293,320 | 4,541,325 | kWh | $0.06 |
Natural Gas | $216,154 | 56,872 | MMBtu | $3.80 |
TOTAL ENERGY COSTS | $509,474 | |||
RECOMMENDED SAVINGS* | $52,730 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $2,279 Cost: $9,740 |
$2,601 | 40,152 | - | - | $(-322) | - |
$2,601 40,152 kWh |
- - MMBtu |
$(-322) - $ |
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02: 2.7122 DISCONNECT BALLASTS |
Savings: $310 Cost: $320 |
$310 | 4,689 | - | - | - | - |
$310 4,689 kWh |
- - MMBtu |
- - $ |
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03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $1,790 Cost: $2,980 |
$1,790 | 27,843 | - | - | - | - |
$1,790 27,843 kWh |
- - MMBtu |
- - $ |
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04: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $848 Cost: $24,790 |
$848 | 13,189 | - | - | - | - |
$848 13,189 kWh |
- - MMBtu |
- - $ |
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05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $3,776 Cost: $150 |
$3,776 | 58,324 | - | - | - | - |
$3,776 58,324 kWh |
- - MMBtu |
- - $ |
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06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $6,747 Cost: $450 |
- | - | $7,197 | 1,894 | $(-450) | - |
- - kWh |
$7,197 1,894 MMBtu |
$(-450) - $ |
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07: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $36,000 Cost: $3,380 |
- | - | $36,000 | 9,473 | - | - |
- - kWh |
$36,000 9,473 MMBtu |
- - $ |
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08: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $980 Cost: $1,880 |
- | - | $980 | 259 | - | - |
- - kWh |
$980 259 MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $52,730 Cost: $43,690 |
$9,325 | 144,197 | $44,177 | 11,626 | $(-772) | - | $9,325 144,197 kWh |
$44,177 11,626 MMBtu |
$(-772) - $ |
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TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - | - | - - kWh |
- - MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |