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IAC Assessment: KU0230
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IAC Assessment: KU0230
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IAC Center Univ. of Kansas
Assessment Year 1987
Principal Product LAB APPARATUS
NAICS n/a
SIC 3821 - Laboratory Apparatus And Furniture
Sales $10,000,000-$50,000,000
# of Employees 200
Plant Area (Sq.Ft.) 0
Annual Production 1,000 Pieces
Production Hrs. Annual 4,160
Location (State) MO
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $138,387 1,676,729 kWh $0.08
Natural Gas $49,291 13,023 MMBtu $3.78
TOTAL ENERGY COSTS $187,678
RECOMMENDED SAVINGS* $16,908 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $7,733
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$4,144
Cost:
$615
$4,144 49,531 - - - - $4,144
49,531
kWh
-
-
MMBtu
-
-
$
02: 2.3191 USE DEMAND CONTROLLER OR LOAD SHEDDER Savings:
$3,808
Cost:
$1,200
$3,808 - - - - - $3,808
-
kWh
-
-
MMBtu
-
-
$
03: 2.2447 HEAT WATER WITH EXHAUST HEAT Savings:
$3,795
Cost:
$7,000
- - $3,795 1,004 - - -
-
kWh
$3,795
1,004
MMBtu
-
-
$
04: 2.1123 INSTALL AUTOMATIC STACK DAMPER Savings:
$1,486
Cost:
$2,600
- - $1,486 393 - - -
-
kWh
$1,486
393
MMBtu
-
-
$
05: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$1,040
Cost:
-
- - $1,300 344 $(-260) - -
-
kWh
$1,300
344
MMBtu
$(-260)
-
$
06: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$677
Cost:
$400
$677 8,206 - - - - $677
8,206
kWh
-
-
MMBtu
-
-
$
07: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$605
Cost:
$90
$605 7,327 - - - - $605
7,327
kWh
-
-
MMBtu
-
-
$
08: 2.6214 SHUT OFF PILOTS IN STANDBY EQUIPMENT Savings:
$437
Cost:
-
- - $537 142 $(-100) - -
-
kWh
$537
142
MMBtu
$(-100)
-
$
09: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$314
Cost:
$205
$314 3,810 - - - - $314
3,810
kWh
-
-
MMBtu
-
-
$
10: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS Savings:
$290
Cost:
$500
$290 3,517 - - - - $290
3,517
kWh
-
-
MMBtu
-
-
$
11: 2.6121 REDUCE HOT WATER TEMPERATURE TO THE MINIMUM REQUIRED Savings:
$191
Cost:
-
- - $191 51 - - -
-
kWh
$191
51
MMBtu
-
-
$
12: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$121
Cost:
$520
$121 1,465 - - - - $121
1,465
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$16,908
Cost:
$13,130
$9,959 73,856 $7,309 1,934 $(-360) - $9,959
73,856
kWh
$7,309
1,934
MMBtu
$(-360)
-
$
TOTAL IMPLEMENTED Savings:
$7,733
Cost:
$3,940
$4,579 54,806 $3,514 930 $(-360) - $4,579
54,806
kWh
$3,514
930
MMBtu
$(-360)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes