Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Univ. of Kansas |
---|---|
Assessment Year | 1990 |
Principal Product | HOMOGINIZED MILK & O.J. |
NAICS | n/a |
SIC | 2026 - Fluid Milk |
Sales | $10,000,000-$50,000,000 |
# of Employees | 225 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 22,000 Thousand Gallons |
Production Hrs. Annual | 7,488 |
Location (State) | MO |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $503,333 | 8,776,378 | kWh | $0.06 |
Natural Gas | $99,370 | 37,089 | MMBtu | $2.68 |
TOTAL ENERGY COSTS | $602,703 | |||
RECOMMENDED SAVINGS* | $63,543 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $30,985 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $20,546 Cost: $12,840 |
$20,546 | 358,441 | - | - | - | - |
$20,546 358,441 kWh |
- - MMBtu |
- - $ |
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02: 2.7263 LOWER COMPRESSOR PRESSURE THROUGH A/C SYSTEM MODIFICATION |
Savings: $10,130 Cost: $10,000 |
$10,130 | 176,729 | - | - | - | - |
$10,130 176,729 kWh |
- - MMBtu |
- - $ |
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03: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $1,042 Cost: $4,000 |
$1,042 | 18,171 | - | - | - | - |
$1,042 18,171 kWh |
- - MMBtu |
- - $ |
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04: 3.4113 TREAT AND REUSE RINSE WATERS |
Savings: $5,895 Cost: $4,000 |
- | - | - | - | $5,895 | - |
- - kWh |
- - MMBtu |
$5,895 - $ |
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05: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $386 Cost: $300 |
$386 | 6,741 | - | - | - | - |
$386 6,741 kWh |
- - MMBtu |
- - $ |
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06: 2.1131 REPAIR FAULTY INSULATION IN FURNACES, BOILERS, ETC |
Savings: $126 Cost: $180 |
- | - | $126 | 47 | - | - |
- - kWh |
$126 47 MMBtu |
- - $ |
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07: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE |
Savings: $22,428 Cost: $20,000 |
$22,428 | 391,266 | - | - | - | - |
$22,428 391,266 kWh |
- - MMBtu |
- - $ |
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08: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $2,990 Cost: $2,400 |
$2,990 | 52,169 | - | - | - | - |
$2,990 52,169 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $63,543 Cost: $53,720 |
$57,522 | 1,003,517 | $126 | 47 | $5,895 | - | $57,522 1,003,517 kWh |
$126 47 MMBtu |
$5,895 - $ |
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TOTAL IMPLEMENTED |
Savings: $30,985 Cost: $23,720 |
$24,964 | 435,522 | $126 | 47 | $5,895 | - | $24,964 435,522 kWh |
$126 47 MMBtu |
$5,895 - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |