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IAC Assessment: KU0336
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IAC Assessment: KU0336
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IAC Center Univ. of Kansas
Assessment Year 1991
Principal Product IND. AIR COMPRESSORS
NAICS n/a
SIC 3564 - Blowers And Fans
Sales $50,000,000-$100,000,000
# of Employees 204
Plant Area (Sq.Ft.) 0
Annual Production 6,120 Pieces
Production Hrs. Annual 5,712
Location (State) MO
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $387,993 7,465,416 kWh $0.05
Natural Gas $76,770 14,411 MMBtu $5.33
TOTAL ENERGY COSTS $464,763
RECOMMENDED SAVINGS* $108,909 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $108,909
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$21,491
Cost:
$19,500
- - $21,491 4,032 - - -
-
kWh
$21,491
4,032
MMBtu
-
-
$
02: 2.7245 USE DIRECT AIR SUPPLY TO EXHAUST HOODS Savings:
$15,055
Cost:
$18,000
$3,137 60,375 $11,918 2,236 - - $3,137
60,375
kWh
$11,918
2,236
MMBtu
-
-
$
03: 2.7243 IMPROVE AIR CIRCULATION WITH DESTRATIFICATION FANS / OTHER METHODS Savings:
$12,114
Cost:
$27,600
$(-838) (-16,120) $12,952 2,430 - - $(-838)
(-16,120)
kWh
$12,952
2,430
MMBtu
-
-
$
04: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$9,818
Cost:
$3,800
- - $9,818 1,842 - - -
-
kWh
$9,818
1,842
MMBtu
-
-
$
05: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME Savings:
$22,099
Cost:
$22,000
$22,099 425,264 - - - - $22,099
425,264
kWh
-
-
MMBtu
-
-
$
06: 2.5194 REDESIGN PROCESS Savings:
$10,585
Cost:
$25,200
$10,585 145,076 - - - - $10,585
145,076
kWh
-
-
MMBtu
-
-
$
07: 2.6221 USE MOST EFFICIENT EQUIPMENT AT IT'S MAXIMUM CAPACITY AND LESS EFFICIENT EQUIPMENT ONLY WHEN NECESSARY Savings:
$5,650
Cost:
$17,100
$5,650 108,734 - - - - $5,650
108,734
kWh
-
-
MMBtu
-
-
$
08: 2.3512 DE-ENERGIZE EXCESS TRANSFORMER CAPACITY Savings:
$1,112
Cost:
-
$1,112 21,395 - - - - $1,112
21,395
kWh
-
-
MMBtu
-
-
$
09: 2.6232 INSTALL SET-BACK TIMERS Savings:
$899
Cost:
$1,000
$899 17,292 - - - - $899
17,292
kWh
-
-
MMBtu
-
-
$
10: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$366
Cost:
-
$366 7,034 - - - - $366
7,034
kWh
-
-
MMBtu
-
-
$
11: 3.4115 RECOVER AND REUSE COOLING WATER Savings:
$9,720
Cost:
$5,340
$(-990) (-19,050) - - $10,710 - $(-990)
(-19,050)
kWh
-
-
MMBtu
$10,710
-
$
TOTAL RECOMMENDED Savings:
$108,909
Cost:
$139,540
$42,020 750,000 $56,179 10,540 $10,710 - $42,020
750,000
kWh
$56,179
10,540
MMBtu
$10,710
-
$
TOTAL IMPLEMENTED Savings:
$108,909
Cost:
$139,540
$42,020 750,000 $56,179 10,540 $10,710 - $42,020
750,000
kWh
$56,179
10,540
MMBtu
$10,710
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes