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IAC Assessment: LM0082
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IAC Assessment: LM0082
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IAC Center Loyola Marymount University
Assessment Year 2004
Principal Product croutons
NAICS 311821 - Cookie and Cracker Manufacturing
SIC 2052 - Cookies And Crackers
Sales $50,000,000-$100,000,000
# of Employees 125
Plant Area (Sq.Ft.) 200,000
Annual Production 33,000,000 Pounds
Production Hrs. Annual 4,680
Location (State) CA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $193,360 1,803,923 kWh $0.11
Electricity Demand $32,966 4,032 kW-months/year $8.18
Electricity Fees $3,856 - $ -
Natural Gas $252,201 39,776 MMBtu $6.34
TOTAL ENERGY COSTS $482,383
RECOMMENDED SAVINGS* $28,291 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Electricity Demand Natural Gas Personnel Changes Electricity Usage Electricity Demand Natural Gas Personnel Changes
$ kWh $ kW-months/year $ MMBtu $ $
01: 2.2511 INSULATE BARE EQUIPMENT Savings:
$13,838
Cost:
$26,170
- - - - $13,838 2,223 - - -
-
kWh
-
-
kW-months/year
$13,838
2,223
MMBtu
-
-
$
02: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$474
Cost:
$65
$402 3,720 $72 8 - - - - $402
3,720
kWh
$72
8
kW-months/year
-
-
MMBtu
-
-
$
03: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$123
Cost:
$169
$88 1,343 $35 4 - - - - $88
1,343
kWh
$35
4
kW-months/year
-
-
MMBtu
-
-
$
04: 4.4320 CROSS-TRAIN PERSONNEL TO AVOID LOST TIME Savings:
$13,000
Cost:
$5,400
- - - - - - $13,000 - -
-
kWh
-
-
kW-months/year
-
-
MMBtu
$13,000
-
$
05: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$856
Cost:
-
$718 6,660 $138 17 - - - - $718
6,660
kWh
$138
17
kW-months/year
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$28,291
Cost:
$31,804
$1,208 11,723 $245 29 $13,838 2,223 $13,000 - $1,208
11,723
kWh
$245
29
kW-months/year
$13,838
2,223
MMBtu
$13,000
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - - - -
-
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ kW-months/year $ MMBtu $ $
Electricity Usage Electricity Demand Natural Gas Personnel Changes Electricity Usage Electricity Demand Natural Gas Personnel Changes