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IAC Assessment: MA0029
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IAC Assessment: MA0029
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IAC Center University of Massachusetts
Assessment Year 1985
Principal Product CORRUG SHIPPING CONTAINERS
NAICS n/a
SIC 2631 - Paperboard Mills
Sales $10,000,000-$50,000,000
# of Employees 70
Plant Area (Sq.Ft.) 0
Annual Production 348,000 Thousand Feet
Production Hrs. Annual 6,732
Location (State) NH
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $145,060 1,886,284 kWh $0.08
Natural Gas $53,813 10,675 MMBtu $5.04
Fuel Oil #4 $14,690 2,419 MMBtu $6.07
Fuel Oil #6 $87,779 17,792 MMBtu $4.93
TOTAL ENERGY COSTS $301,342
RECOMMENDED SAVINGS* $34,037 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Fuel Oil #6 Electricity Usage Natural Gas Fuel Oil #6
$ kWh $ MMBtu $ MMBtu
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$344
Cost:
$94
$344 4,396 - - - - $344
4,396
kWh
-
-
MMBtu
-
-
MMBtu
02: 2.7245 USE DIRECT AIR SUPPLY TO EXHAUST HOODS Savings:
$17,454
Cost:
$9,015
- - $6,638 1,317 $10,816 2,194 -
-
kWh
$6,638
1,317
MMBtu
$10,816
2,194
MMBtu
03: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$6,980
Cost:
$268
- - $2,651 526 $4,329 878 -
-
kWh
$2,651
526
MMBtu
$4,329
878
MMBtu
04: 2.6242 MINIMIZE OPERATION OF EQUIPMENT MAINTAINED IN STANDBY CONDITION Savings:
$636
Cost:
$763
- - $242 48 $394 80 -
-
kWh
$242
48
MMBtu
$394
80
MMBtu
05: 2.5123 REDUCE FLUID FLOW RATES Savings:
$2,655
Cost:
-
- - $1,008 200 $1,647 334 -
-
kWh
$1,008
200
MMBtu
$1,647
334
MMBtu
06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$5,968
Cost:
$2,000
- - $2,268 450 $3,700 751 -
-
kWh
$2,268
450
MMBtu
$3,700
751
MMBtu
TOTAL RECOMMENDED Savings:
$34,037
Cost:
$12,140
$344 4,396 $12,807 2,541 $20,886 4,237 $344
4,396
kWh
$12,807
2,541
MMBtu
$20,886
4,237
MMBtu
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - -
-
kWh
-
-
MMBtu
-
-
MMBtu
Savings
Cost
$ kWh $ MMBtu $ MMBtu
Electricity Usage Natural Gas Fuel Oil #6 Electricity Usage Natural Gas Fuel Oil #6