Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Massachusetts |
---|---|
Assessment Year | 1992 |
Principal Product | VINYL SHEETING AND FILM |
NAICS | n/a |
SIC | 2295 - Coated Fabrics, Not Rubberized |
Sales | $10,000,000-$50,000,000 |
# of Employees | 116 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 21,000 Thousand Feet |
Production Hrs. Annual | 5,760 |
Location (State) | CT |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $577,279 | 6,085,580 | kWh | $0.09 |
Natural Gas | $116,960 | 35,302 | MMBtu | $3.31 |
Fuel Oil #6 | $44,541 | 16,624 | MMBtu | $2.68 |
TOTAL ENERGY COSTS | $738,780 | |||
RECOMMENDED SAVINGS* | $44,383 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $20,358 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | LPG | Fuel Oil #6 | Electricity Usage | Natural Gas | LPG | Fuel Oil #6 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | MMBtu | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.1331 BURN A LESS EXPENSIVE GRADE OF FUEL |
Savings: $20,512 Cost: - |
- | - | $34,170 | 5,003 | $(-13,658) | (-5,003) | - | - |
- - kWh |
$34,170 5,003 MMBtu |
$(-13,658) (-5,003) MMBtu |
- - MMBtu |
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02: 2.7316 CENTRALIZE CONTROL OF EXHAUST FANS TO ENSURE THEIR SHUTDOWN, OR ESTABLISH PROGRAM TO ENSURE MANUAL SHUTDOWN |
Savings: $10,171 Cost: $100 |
$10,171 | 107,268 | - | - | - | - | - | - |
$10,171 107,268 kWh |
- - MMBtu |
- - MMBtu |
- - MMBtu |
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03: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $4,808 Cost: $6,580 |
$4,808 | 50,703 | - | - | - | - | - | - |
$4,808 50,703 kWh |
- - MMBtu |
- - MMBtu |
- - MMBtu |
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04: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $2,251 Cost: $5,020 |
$2,251 | 23,740 | - | - | - | - | - | - |
$2,251 23,740 kWh |
- - MMBtu |
- - MMBtu |
- - MMBtu |
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05: 2.2122 INSTALL / REPAIR INSULATION ON CONDENSATE LINES |
Savings: $1,845 Cost: $600 |
- | - | $1,263 | 462 | - | - | $582 | 217 |
- - kWh |
$1,263 462 MMBtu |
- - MMBtu |
$582 217 MMBtu |
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06: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $1,480 Cost: $2,854 |
- | - | $1,014 | 371 | - | - | $466 | 174 |
- - kWh |
$1,014 371 MMBtu |
- - MMBtu |
$466 174 MMBtu |
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07: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $1,312 Cost: $300 |
- | - | $950 | 287 | - | - | $362 | 135 |
- - kWh |
$950 287 MMBtu |
- - MMBtu |
$362 135 MMBtu |
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08: 2.1393 USE STEAM SPARGING OR INJECTIONS IN PLACE OF INDIRECT HEATING |
Savings: $742 Cost: $1,668 |
- | - | $536 | 162 | - | - | $206 | 77 |
- - kWh |
$536 162 MMBtu |
- - MMBtu |
$206 77 MMBtu |
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09: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $750 Cost: - |
$750 | 7,913 | - | - | - | - | - | - |
$750 7,913 kWh |
- - MMBtu |
- - MMBtu |
- - MMBtu |
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10: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS |
Savings: $512 Cost: $77 |
$512 | 5,275 | - | - | - | - | - | - |
$512 5,275 kWh |
- - MMBtu |
- - MMBtu |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $44,383 Cost: $17,199 |
$18,492 | 194,899 | $37,933 | 6,285 | $(-13,658) | (-5,003) | $1,616 | 603 | $18,492 194,899 kWh |
$37,933 6,285 MMBtu |
$(-13,658) (-5,003) MMBtu |
$1,616 603 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $20,358 Cost: $12,102 |
$14,979 | 157,971 | $3,763 | 1,282 | - | - | $1,616 | 603 | $14,979 157,971 kWh |
$3,763 1,282 MMBtu |
- - MMBtu |
$1,616 603 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | MMBtu | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | LPG | Fuel Oil #6 | Electricity Usage | Natural Gas | LPG | Fuel Oil #6 |