Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Missouri, Rolla |
---|---|
Assessment Year | 1994 |
Principal Product | Remanufacture of Aircraft Engines |
NAICS | n/a |
SIC | 3599 - Industrial Machinery, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 125 |
Plant Area (Sq.Ft.) | 325,000 |
Annual Production | 98,496 Pieces |
Production Hrs. Annual | 2,040 |
Location (State) | MO |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $258,955 | 6,197,538 | kWh | $0.04 |
Natural Gas | $82,374 | 34,929 | MMBtu | $2.36 |
TOTAL ENERGY COSTS | $341,329 | |||
RECOMMENDED SAVINGS* | $22,872 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $342 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.3113 MAKE ICE DURING OFF PEAK HOURS FOR COOLING |
Savings: $11,331 Cost: $33,300 |
$(-521) | (-12,603) | - | - | $11,852 | - |
$(-521) (-12,603) kWh |
- - MMBtu |
$11,852 - $ |
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02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $8,025 Cost: $41,137 |
$8,025 | 191,970 | - | - | - | - |
$8,025 191,970 kWh |
- - MMBtu |
- - $ |
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03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $1,632 Cost: $1,236 |
$1,632 | 38,980 | - | - | - | - |
$1,632 38,980 kWh |
- - MMBtu |
- - $ |
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04: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $766 Cost: $645 |
$766 | 18,171 | - | - | - | - |
$766 18,171 kWh |
- - MMBtu |
- - $ |
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05: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $678 Cost: $3,209 |
$678 | 16,120 | - | - | - | - |
$678 16,120 kWh |
- - MMBtu |
- - $ |
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06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $342 Cost: $995 |
- | - | $342 | 143 | - | - |
- - kWh |
$342 143 MMBtu |
- - $ |
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07: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $98 Cost: $30 |
$98 | 2,345 | - | - | - | - |
$98 2,345 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $22,872 Cost: $80,552 |
$10,678 | 254,983 | $342 | 143 | $11,852 | - | $10,678 254,983 kWh |
$342 143 MMBtu |
$11,852 - $ |
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TOTAL IMPLEMENTED |
Savings: $342 Cost: $995 |
- | - | $342 | 143 | - | - | - - kWh |
$342 143 MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |