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IAC Assessment: OK0229
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IAC Assessment: OK0229
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Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
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IAC Center Oklahoma State University
Assessment Year 1987
Principal Product INJECTION MOLDINGS
NAICS n/a
SIC 3089 - Plastics Products, Nec
Sales $50,000,000-$100,000,000
# of Employees 250
Plant Area (Sq.Ft.) 0
Annual Production 0 Units
Production Hrs. Annual 4,500
Location (State) OK
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $151,395 2,596,424 kWh $0.06
Natural Gas $20,908 4,963 MMBtu $4.21
TOTAL ENERGY COSTS $172,303
RECOMMENDED SAVINGS* $14,875 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $5,491
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$114
Cost:
-
$154 4,396 - - $(-40) - $154
4,396
kWh
-
-
MMBtu
$(-40)
-
$
02: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$577
Cost:
-
- - $577 137 - - -
-
kWh
$577
137
MMBtu
-
-
$
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$433
Cost:
-
$433 6,155 - - - - $433
6,155
kWh
-
-
MMBtu
-
-
$
04: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS Savings:
$1,236
Cost:
$1,031
$1,236 23,740 - - - - $1,236
23,740
kWh
-
-
MMBtu
-
-
$
05: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$3,708
Cost:
$2,200
$3,708 - - - - - $3,708
-
kWh
-
-
MMBtu
-
-
$
06: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES Savings:
$3,856
Cost:
$1,100
$3,856 109,320 - - - - $3,856
109,320
kWh
-
-
MMBtu
-
-
$
07: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS Savings:
$4,951
Cost:
$3,660
$4,951 80,891 - - - - $4,951
80,891
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$14,875
Cost:
$7,991
$14,338 224,502 $577 137 $(-40) - $14,338
224,502
kWh
$577
137
MMBtu
$(-40)
-
$
TOTAL IMPLEMENTED Savings:
$5,491
Cost:
$3,231
$5,531 34,291 - - $(-40) - $5,531
34,291
kWh
-
-
MMBtu
$(-40)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes