Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oklahoma State University |
---|---|
Assessment Year | 1987 |
Principal Product | INJECTION MOLDINGS |
NAICS | n/a |
SIC | 3089 - Plastics Products, Nec |
Sales | $50,000,000-$100,000,000 |
# of Employees | 250 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 0 Units |
Production Hrs. Annual | 4,500 |
Location (State) | OK |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $151,395 | 2,596,424 | kWh | $0.06 |
Natural Gas | $20,908 | 4,963 | MMBtu | $4.21 |
TOTAL ENERGY COSTS | $172,303 | |||
RECOMMENDED SAVINGS* | $14,875 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $5,491 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $114 Cost: - |
$154 | 4,396 | - | - | $(-40) | - |
$154 4,396 kWh |
- - MMBtu |
$(-40) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $577 Cost: - |
- | - | $577 | 137 | - | - |
- - kWh |
$577 137 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $433 Cost: - |
$433 | 6,155 | - | - | - | - |
$433 6,155 kWh |
- - MMBtu |
- - $ |
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04: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $1,236 Cost: $1,031 |
$1,236 | 23,740 | - | - | - | - |
$1,236 23,740 kWh |
- - MMBtu |
- - $ |
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05: 2.3212 OPTIMIZE PLANT POWER FACTOR |
Savings: $3,708 Cost: $2,200 |
$3,708 | - | - | - | - | - |
$3,708 - kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
06: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES |
Savings: $3,856 Cost: $1,100 |
$3,856 | 109,320 | - | - | - | - |
$3,856 109,320 kWh |
- - MMBtu |
- - $ |
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07: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $4,951 Cost: $3,660 |
$4,951 | 80,891 | - | - | - | - |
$4,951 80,891 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $14,875 Cost: $7,991 |
$14,338 | 224,502 | $577 | 137 | $(-40) | - | $14,338 224,502 kWh |
$577 137 MMBtu |
$(-40) - $ |
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TOTAL IMPLEMENTED |
Savings: $5,491 Cost: $3,231 |
$5,531 | 34,291 | - | - | $(-40) | - | $5,531 34,291 kWh |
- - MMBtu |
$(-40) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |