Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oklahoma State University |
---|---|
Assessment Year | 1987 |
Principal Product | SWITCHES & GAUGES |
NAICS | n/a |
SIC | 3613 - Switchgear And Switchboard Apparatus |
Sales | $10,000,000-$50,000,000 |
# of Employees | 200 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 180,000 Pieces |
Production Hrs. Annual | 2,340 |
Location (State) | OK |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $46,877 | 691,970 | kWh | $0.07 |
Natural Gas | $10,071 | 2,024 | MMBtu | $4.98 |
TOTAL ENERGY COSTS | $56,948 | |||
RECOMMENDED SAVINGS* | $6,328 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $6,328 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $759 Cost: $238 |
$822 | 13,189 | $(-63) | (-17) | - | - |
$822 13,189 kWh |
$(-63) (-17) MMBtu |
- - $ |
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02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $353 Cost: $734 |
$382 | 5,862 | $(-29) | (-8) | - | - |
$382 5,862 kWh |
$(-29) (-8) MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $241 Cost: $80 |
$241 | 5,862 | - | - | - | - |
$241 5,862 kWh |
- - MMBtu |
- - $ |
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04: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS |
Savings: $2,644 Cost: $3,300 |
- | - | $2,644 | 604 | - | - |
- - kWh |
$2,644 604 MMBtu |
- - $ |
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05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $283 Cost: - |
$343 | 11,137 | - | - | $(-60) | - |
$343 11,137 kWh |
- - MMBtu |
$(-60) - $ |
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06: 2.8112 COMBINE UTILITY METERS |
Savings: $768 Cost: $520 |
- | - | $768 | - | - | - |
- - kWh |
$768 - MMBtu |
- - $ |
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07: 2.3191 USE DEMAND CONTROLLER OR LOAD SHEDDER |
Savings: $1,280 Cost: $820 |
$1,280 | - | - | - | - | - |
$1,280 - kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $6,328 Cost: $5,692 |
$3,068 | 36,050 | $3,320 | 579 | $(-60) | - | $3,068 36,050 kWh |
$3,320 579 MMBtu |
$(-60) - $ |
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TOTAL IMPLEMENTED |
Savings: $6,328 Cost: $5,692 |
$3,068 | 36,050 | $3,320 | 579 | $(-60) | - | $3,068 36,050 kWh |
$3,320 579 MMBtu |
$(-60) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |