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IAC Assessment: OK0236
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IAC Assessment: OK0236
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Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
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IAC Center Oklahoma State University
Assessment Year 1987
Principal Product SWITCHES & GAUGES
NAICS n/a
SIC 3613 - Switchgear And Switchboard Apparatus
Sales $10,000,000-$50,000,000
# of Employees 200
Plant Area (Sq.Ft.) 0
Annual Production 180,000 Pieces
Production Hrs. Annual 2,340
Location (State) OK
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $46,877 691,970 kWh $0.07
Natural Gas $10,071 2,024 MMBtu $4.98
TOTAL ENERGY COSTS $56,948
RECOMMENDED SAVINGS* $6,328 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $6,328
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$759
Cost:
$238
$822 13,189 $(-63) (-17) - - $822
13,189
kWh
$(-63)
(-17)
MMBtu
-
-
$
02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$353
Cost:
$734
$382 5,862 $(-29) (-8) - - $382
5,862
kWh
$(-29)
(-8)
MMBtu
-
-
$
03: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS Savings:
$241
Cost:
$80
$241 5,862 - - - - $241
5,862
kWh
-
-
MMBtu
-
-
$
04: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS Savings:
$2,644
Cost:
$3,300
- - $2,644 604 - - -
-
kWh
$2,644
604
MMBtu
-
-
$
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$283
Cost:
-
$343 11,137 - - $(-60) - $343
11,137
kWh
-
-
MMBtu
$(-60)
-
$
06: 2.8112 COMBINE UTILITY METERS Savings:
$768
Cost:
$520
- - $768 - - - -
-
kWh
$768
-
MMBtu
-
-
$
07: 2.3191 USE DEMAND CONTROLLER OR LOAD SHEDDER Savings:
$1,280
Cost:
$820
$1,280 - - - - - $1,280
-
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$6,328
Cost:
$5,692
$3,068 36,050 $3,320 579 $(-60) - $3,068
36,050
kWh
$3,320
579
MMBtu
$(-60)
-
$
TOTAL IMPLEMENTED Savings:
$6,328
Cost:
$5,692
$3,068 36,050 $3,320 579 $(-60) - $3,068
36,050
kWh
$3,320
579
MMBtu
$(-60)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes