Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oklahoma State University |
---|---|
Assessment Year | 1987 |
Principal Product | WESTERN WEAR CLOTHING |
NAICS | n/a |
SIC | 2329 - Men's and Boys' Clothing, Not Elsewhere Classified |
Sales | $1,000,000-$5,000,000 |
# of Employees | 65 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 0 Units |
Production Hrs. Annual | 2,340 |
Location (State) | OK |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $17,895 | 237,397 | kWh | $0.08 |
Natural Gas | $10,045 | 2,338 | MMBtu | $4.30 |
TOTAL ENERGY COSTS | $27,940 | |||
RECOMMENDED SAVINGS* | $5,215 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $2,520 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $1,960 Cost: $6,525 |
$1,960 | 22,274 | - | - |
$1,960 22,274 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $148 Cost: $71 |
$148 | 586 | - | - |
$148 586 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $297 Cost: $288 |
- | - | $297 | 69 |
- - kWh |
$297 69 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
04: 2.7221 LOWER TEMPERATURE DURING THE WINTER SEASON AND VICE-VERSA |
Savings: $1,273 Cost: $1,050 |
- | - | $1,273 | 296 |
- - kWh |
$1,273 296 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 2.7252 UTILIZE AN EVAPORATIVE AIR PRE-COOLER OR OTHER HEAT EXCHANGER IN AC SYSTEM |
Savings: $735 Cost: $2,083 |
$735 | 7,913 | - | - |
$735 7,913 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
06: 2.1222 INSTALL TURBULATORS |
Savings: $108 Cost: $220 |
- | - | $108 | 25 |
- - kWh |
$108 25 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
07: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED |
Savings: $82 Cost: $220 |
- | - | $82 | 16 |
- - kWh |
$82 16 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
08: 2.2111 INSTALL STEAM TRAP |
Savings: $612 Cost: $1,950 |
- | - | $612 | 142 |
- - kWh |
$612 142 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $5,215 Cost: $12,407 |
$2,843 | 30,773 | $2,372 | 548 | $2,843 30,773 kWh |
$2,372 548 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $2,520 Cost: $3,799 |
$148 | 586 | $2,372 | 548 | $148 586 kWh |
$2,372 548 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |