Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oklahoma State University |
---|---|
Assessment Year | 2010 |
Principal Product | Poultry Processing and Packaging |
NAICS | 311615 - Poultry Processing |
SIC | 2015 - Poultry Slaughtering And Processing |
Sales | $100,000,000-$500,000,000 |
# of Employees | 100 |
Plant Area (Sq.Ft.) | 116,000 |
Annual Production | 112,000,000 Pieces |
Production Hrs. Annual | 4,160 |
Location (State) | OK |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $1,560,589 | 24,772,800 | kWh | $0.06 |
Electricity Demand | $341,721 | 56,588 | kW-months/year | $6.04 |
Natural Gas | $859,781 | 183,413 | MMBtu | $4.69 |
TOTAL ENERGY COSTS | $3,782,505 | |||
RECOMMENDED SAVINGS* | $201,081 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $17,592 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT |
Savings: $80,818 Cost: $182,391 |
- | - | $80,818 | 14,984 |
- - kWh |
$80,818 14,984 MMBtu |
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02: 2.2691 SHUT OFF COOLING IF COLD OUTSIDE AIR WILL COOL PROCESS |
Savings: $20,004 Cost: $15,450 |
$20,004 | 318,036 | - | - |
$20,004 318,036 kWh |
- - MMBtu |
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03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $7,970 Cost: $31,888 |
$7,970 | 126,703 | - | - |
$7,970 126,703 kWh |
- - MMBtu |
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04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $13,476 Cost: $144,256 |
$13,476 | 214,250 | - | - |
$13,476 214,250 kWh |
- - MMBtu |
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05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $384 Cost: $1,579 |
$384 | 6,098 | - | - |
$384 6,098 kWh |
- - MMBtu |
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06: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $7,798 Cost: $7,980 |
$7,798 | 127,164 | - | - |
$7,798 127,164 kWh |
- - MMBtu |
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07: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $23,330 Cost: $17,280 |
$23,330 | 370,913 | - | - |
$23,330 370,913 kWh |
- - MMBtu |
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08: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $827 Cost: $896 |
- | - | $827 | 176 |
- - kWh |
$827 176 MMBtu |
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09: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $10,734 Cost: $5,136 |
$10,734 | 170,654 | - | - |
$10,734 170,654 kWh |
- - MMBtu |
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10: 2.3137 USE POWER DURING OFF-PEAK PERIODS |
Savings: $34,743 Cost: $99,978 |
$34,743 | 273,575 | - | - |
$34,743 273,575 kWh |
- - MMBtu |
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11: 2.3132 RECHARGE BATTERIES ON DURING OFF-PEAK DEMAND PERIODS |
Savings: $997 Cost: $1,486 |
$997 | - | - | - |
$997 - kWh |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $201,081 Cost: $508,320 |
$119,436 | 1,607,393 | $81,645 | 15,160 | $119,436 1,607,393 kWh |
$81,645 15,160 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $17,592 Cost: $42,250 |
$16,765 | 253,867 | $827 | 176 | $16,765 253,867 kWh |
$827 176 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |