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IAC Assessment: OK0840
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IAC Assessment: OK0840
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Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
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IAC Center Oklahoma State University
Assessment Year 2013
Principal Product Carbinated beverages
NAICS 312111 - Soft Drink Manufacturing
SIC 2086 - Bottled And Canned Soft Drinks
Sales $5,000,000-$10,000,000
# of Employees 125
Plant Area (Sq.Ft.) 500,000
Annual Production 7,000,000 Units
Production Hrs. Annual 2,600
Location (State) TX
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $275,164 3,633,887 kWh $0.08
Natural Gas $37,106 8,691 MMBtu $4.27
TOTAL ENERGY COSTS $312,270
RECOMMENDED SAVINGS* $50,143 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $27,331
#|Description Savings
Cost
Status Electricity Usage Natural Gas Electricity Usage Natural Gas
$ kWh $ MMBtu
01: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$3,788
Cost:
$27,500
$3,788 49,838 - - $3,788
49,838
kWh
-
-
MMBtu
02: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$2,073
Cost:
$600
$2,073 27,276 - - $2,073
27,276
kWh
-
-
MMBtu
03: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$1,413
Cost:
$1,378
- - $1,413 330 -
-
kWh
$1,413
330
MMBtu
04: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$1,327
Cost:
-
$1,327 17,456 - - $1,327
17,456
kWh
-
-
MMBtu
05: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS Savings:
$360
Cost:
$1,575
$360 4,731 - - $360
4,731
kWh
-
-
MMBtu
06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$673
Cost:
$8,267
$673 8,850 - - $673
8,850
kWh
-
-
MMBtu
07: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$1,885
Cost:
$7,053
$1,885 24,480 - - $1,885
24,480
kWh
-
-
MMBtu
08: 2.1224 REPLACE BOILER Savings:
$6,063
Cost:
$60,000
- - $6,063 1,420 -
-
kWh
$6,063
1,420
MMBtu
09: 2.7232 REPLACE EXISTING HVAC UNIT WITH HIGH EFFICIENCY MODEL Savings:
$5,770
Cost:
$21,632
$5,770 75,923 - - $5,770
75,923
kWh
-
-
MMBtu
10: 2.1231 ESTABLISH BURNER MAINTENANCE SCHEDULE FOR BOILERS Savings:
$1,310
Cost:
$4,958
$1,310 16,374 - - $1,310
16,374
kWh
-
-
MMBtu
11: 2.7241 INSTALL OUTSIDE AIR DAMPER / ECONOMIZER ON HVAC UNIT Savings:
$3,220
Cost:
$3,650
$3,220 42,360 - - $3,220
42,360
kWh
-
-
MMBtu
12: 2.6232 INSTALL SET-BACK TIMERS Savings:
$2,987
Cost:
$2,259
$1,884 24,789 $1,103 258 $1,884
24,789
kWh
$1,103
258
MMBtu
13: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES Savings:
$4,448
Cost:
-
$4,448 58,522 - - $4,448
58,522
kWh
-
-
MMBtu
14: 2.4131 SIZE ELECTRIC MOTORS FOR PEAK OPERATING EFFICIENCY Savings:
$14,826
Cost:
$25,000
$14,826 195,075 - - $14,826
195,075
kWh
-
-
MMBtu
TOTAL RECOMMENDED Savings:
$50,143
Cost:
$163,872
$41,564 545,674 $8,579 2,008 $41,564
545,674
kWh
$8,579
2,008
MMBtu
TOTAL IMPLEMENTED Savings:
$27,331
Cost:
$34,392
$26,228 344,223 $1,103 258 $26,228
344,223
kWh
$1,103
258
MMBtu
Savings
Cost
$ kWh $ MMBtu
Electricity Usage Natural Gas Electricity Usage Natural Gas