Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oregon State University |
---|---|
Assessment Year | 1988 |
Principal Product | PACKAGED SEAFOOD |
NAICS | n/a |
SIC | 2092 - Fresh Or Frozen Prepared Fish |
Sales | $10,000,000-$50,000,000 |
# of Employees | 40 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 29,000,000 Pounds |
Production Hrs. Annual | 8,736 |
Location (State) | OR |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $181,760 | 4,177,902 | kWh | $0.04 |
Natural Gas | $97,865 | 20,844 | MMBtu | $4.70 |
TOTAL ENERGY COSTS | $279,625 | |||
RECOMMENDED SAVINGS* | $9,966 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $5,625 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE |
Savings: $767 Cost: - |
$767 | 17,585 | - | - | - | - |
$767 17,585 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $3,744 Cost: $300 |
- | - | $3,744 | 823 | - | - |
- - kWh |
$3,744 823 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $279 Cost: $167 |
$279 | 6,448 | - | - | - | - |
$279 6,448 kWh |
- - MMBtu |
- - $ |
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04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $575 Cost: $878 |
$417 | 9,379 | - | - | $158 | - |
$417 9,379 kWh |
- - MMBtu |
$158 - $ |
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05: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $260 Cost: $295 |
$304 | 7,034 | - | - | $(-44) | - |
$304 7,034 kWh |
- - MMBtu |
$(-44) - $ |
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06: 2.3212 OPTIMIZE PLANT POWER FACTOR |
Savings: $2,051 Cost: $4,500 |
$2,051 | - | - | - | - | - |
$2,051 - kWh |
- - MMBtu |
- - $ |
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07: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $2,290 Cost: $7,790 |
- | - | $2,290 | 503 | - | - |
- - kWh |
$2,290 503 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $9,966 Cost: $13,930 |
$3,818 | 40,446 | $6,034 | 1,326 | $114 | - | $3,818 40,446 kWh |
$6,034 1,326 MMBtu |
$114 - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $5,625 Cost: $1,640 |
$1,767 | 40,446 | $3,744 | 823 | $114 | - | $1,767 40,446 kWh |
$3,744 823 MMBtu |
$114 - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |